UNITED STATES
DEPARTMENT OF LABOR
MINE SAFETY AND HEALTH ADMINISTRATION
District 11
ACCIDENT INVESTIGATION REPORT
Surface Area of Underground Mine
Fall of Material
Structural Failure
No. 5 Mine, I. D. No. 01-01322
Jim Walter Resources, Incorporated
Brookwood, Tuscaloosa County, Alabama
November 10, 1995
By
Walter W. Deason
Coal Mine Inspector
Donald T. Kirkwood
Civil Engineer, Pittsburgh Safety and Health Tech. Center
Terence M. Taylor
Civil Engineer, Pittsburgh Safety and Health Tech. Center
Originating Office - Mine Safety and Health Administration
135 Gemini Circle, Suite 213, Birmingham, Alabama 35209-5842
Michael J. Lawless, District Manager
GENERAL INFORMATION
The No. 5 Mine, Jim Walter Resources, Incorporated, is located in
Brookwood, Tuscaloosa County, Alabama. This is a vertical shaft
mine approximately 2,100 to 2,500 feet in depth which liberates
approximately 20,000,000 cubic feet of methane in a 24-hour
period. The mine has three continuous mining machine sections on
development work and one longwall section on retreat mining. The
mine employs 373 miners and has a daily production of 8,000 to
10,000 tons of raw coal. The preparation plant operates two to
three shifts per day, five to six days per week. The preparation
plant processes 4,477 tons of coal daily, with a washer reject of
44 percent. The last completed Mine Safety and Health
Administration health and safety inspection was conducted from
July to September 1995. An ongoing Mine Safety and Health
Administration health and safety inspection is being conducted
which began in October, 1995.
Company officials are listed below:
William Carr.......................................President
K. J. Matlock......................................Vice President
James M. Smith....................................Vice President
W. H. Weldon.....................................Treasurer
John F. Turbiville...................................Secretary
DESCRIPTION OF THE ACCIDENT
On Friday, November 10, 1995 at approximately 7:00 a.m., the day
shift preparation plant crew gathered in the dining area of the
plant and C.A. Squire, Plant Foreman, gave out the work
assignments.
Thomas Alton Emfinger, Heavy Equipment Operator (victim) and
Ronald Holmes, Heavy Equipment Operator, were assigned to haul
refuse rock from the refuse bin. Normal haulage operations
continued throughout the morning. The cab door on the rock truck
that Emfinger was operating would not stay closed, so he took the
truck to the shop to be repaired. He obtained an International
330 rock truck and returned to the rock bin area.
Emfinger and Holmes took turns eating lunch. After lunch, they
emptied the rock bin. Holmes left the rock bin area to get fuel
for his Terex Pan. When Holmes returned to the rock bin,
Emfinger was parked out from beneath the rock bin on the west
side. Holmes pulled his pan to within 30 feet of the rock bin on
the east side. Holmes sat there for approximately ten minutes
and at approximately 12:45 p.m., Emfinger backed his truck
beneath the rock bin. Holmes stated that when the rock chute
door started to open, he saw and heard the cone section of the
rock bin begin to fall and land on the cab of Emfinger's rock
truck.
There were approximately 150 tons of refuse rock in the bin. The
weight broke the front axle on the truck and mashed the cab and
frame down toward the ground and the rock covered the cab area
where Emfinger was located.
There were no communication devices in the pan so Holmes drove to
the washer area for help. Rescue efforts began and the victim
was trapped in the cab of the rock truck for approximately two
hours and 53 minutes. He was pronounced dead on the scene by the
doctor in attendance.
PHYSICAL FACTORS INVOLVED IN THE ACCIDENT
Original Structure
The refuse bin at Jim Walter Resources, Inc., Mine No. 5 was
designed and constructed by McNally Pittsburg Manufacturing
Corporation. According to the dates on the design drawings No.
E-4801-42, E-4801-43, and E-4801-44 the refuse bin was
constructed in 1976 and 1977. The refuse bin structure is 70
feet high and consists of four main support columns. They
support the 300-ton refuse bin, a hydraulically operated gate
mechanism at the bottom of the cone, the end section of the 36
inch wide refuse conveyor belt and supporting structure, and an
enclosure housing the conveyor belt head drive, motors, and
controls. The compass direction north is on the side of the bin
opposite the conveyor structure. The conveyor structure attaches
to the bin at a point approximately 58 feet above the column
base. For clarity, the four main columns will be referred to as
the northeast, northwest, southeast, and southwest columns. The
vehicular traffic pulled under the bin from the east toward the
west.
McNally Pittsburgh's Drawing No. E-4801-42 identifies the refuse
bin as a 300-ton capacity structure with typical refuse material
listed as having a unit weight of 100 lbs./cu.ft. Using the 100
lbs./cu. ft. weight and the calculated volume of the refuse bin
including the cone and cylinder sections, the estimated weight
for a fully loaded bin would have been in excess of 340 tons.
The four columns were designed as W10x49 steel sections for the
bottom 42 feet and W10x33 sections for the upper 28 feet. The
main horizontal steel members which extend between the four
columns, were designated as W12x27 sections 18 feet above the
column base (design drawing elevation 151 feet), W21x55 sections
40 feet above the column base (elevation 173 feet 3 inches ),
W18x45 sections 58 feet above the column base (elevation 191 feet
7 inches), and W10X21 sections supporting the roof approximately
70 feet above the column base (elevation 203 feet 6 inches).
The refuse conveyor belt dumped the rock and refuse into the bin
at drawing elevation 194 feet. The material dropped through an
opening in the floor at the elevation 191 feet 7 inches, which
was 11 1/2 inches beneath the end of the belt. The refuse bin
consists of two main sections. The upper section of the refuse
bin was a 12 feet high, 21 feet 10 inches in diameter, steel
cylinder constructed out of 1/4 inch thick steel plates. Welded
beneath this cylinder was a truncated, steel cone. The cone was
15 feet 6 inches high and had a 4 foot diameter opening in its
bottom. The cone was constructed of 1/4 inch plate steel with
1/4 inch hardened steel liners along the inside. The gate for
regulating the flow of material from the bin was attached to the
bottom of the cone.
At the drawing elevation 173 feet 3 inches, four W21x73 sections
were connected across the corners of the main W21x55 beams
forming an equilateral octagon with 9 feet 6 3/8 inch long sides.
The compression ring beam was composed of two 1/2 inch plates
acting as flanges and the section of the 1/4 inch cylinder plate
between them, acting as the web. The bottom flange of the
compression ring beam rested on the beams forming this octagon.
This 1/2 inch compression ring bottom flange was welded
perpendicular (horizontal) to the vertical, 1/4 inch cylinder
plate approximately 3 inches above the bottom of the cylinder
plate. A second 1/2 inch horizontal plate was welded around the
circumference of the vertical cylinder plate, 2 feet above the
first plate. The compression ring beam also had sixteen, 1/2
inch thick, vertical, bearing stiffener plates welded between its
upper and lower flanges. These stiffeners were placed in pairs,
one foot apart, centered over the eight locations where the lower
flange of the compression ring beam rested fully over the 21-inch
deep beam comprising the octagon. The cone section was welded to
the inside of the cylinder plate at the same level that the lower
flange of the compression ring beam was welded to the outside of
the cylinder plate.
The forces exerted by the weight of the waste rock inside of the
bin and the weight of the cone and its liners were carried
through the cone, to the compression ring beam. The compression
beam was supported by the octagon shaped frame of the 21 inch
deep beams. The forces in the octagon beams were then
transmitted down through the four main columns. The compression
ring beam also supported the cylinder section laterally against
the forces of the material inside the cone.
The bin was designed so that mobile equipment could enter either
from the east or west side between the main columns. The trucks
would pull directly under the center of the cone. The gate would
be opened remotely and the truck would be filled with refuse and
rock. The gate would then be closed remotely, and the truck
would exit. No indicators of the material level within the bin
were originally installed, nor required. The bin was later
equipped with a high level rock indicator.
1991 Modification
The size of the material that was dumped into the refuse bin
varied from fine dust to large, 18 inch rocks. The refuse and
rocks were dumped from the conveyor belt at a height of 37 feet
above the bottom of the cone. The impact of the large rocks on
the cone, the abrasion from sliding material, and the corrosive
nature of the wet, acidic environment within the bin led to
continual deterioration of the inside of the bin. The area that
would deteriorate most rapidly was the inside of the cone section
and that is why the cone was fitted with hardened steel, armor
plates on its inside. Despite the additional protection afforded
by these armor or wear plates, the cone section was typically the
first area to show signs of serious wear or deterioration.
To address this problem, in 1991 Jim Walter Resources designed a
modification to the bin which would allow the cone and its liner
plates to be periodically replaced. This modification is
illustrated on the design drawings prepared by JWR's designer Ira
Lanstrum, numbered 735 A-71355, 735 A-71356, and 735 A-71357.
These drawings are identified as applying to the refuse bin at
JWR's No. 7 Mine, however, the company stated that they were also
used in the fabrication and installation of the refuse bin
modification at JWR's No. 5 Mine in 1991. Selman Fabricators
assembled the replacement cone sections in 1991 and Professional
Iron Workers (PIW) installed the cone in July 1991.
The modification (Dwg. 735 A-71355) called for cutting the
original cone off at a point 7 5/16 inches below the attachment
point of the cone to the cylinder, described above. A steel
flange (top flange) 1/4 inch thick, and 48 gusset plates were
welded to the bottom of the section of original cone at the cut
line. The drawings called for the top flange to have 136, 13/16
inch diameter bolt holes drilled on 6 inch centers.
In 1991, the cone was fabricated in two sections, an upper cone
section and a lower cone section. The upper cone section (Dwg.
735 A-71357) was fabricated in eight tapered and curved segments.
Each segment was 9 feet 10 13/16 inches high, 8 1/2 feet wide on
its top, and 4 feet wide on its bottom. Each of the eight
segments had flanges welded to its top and bottom. The drawings
called for both flanges to have 13/16 inch diameter bolt holes
drilled through them on 6 inch centers. Another flange was
welded to each side of each upper cone segment. The side flanges
also had 13/16 inch diameter bolt holes drilled through them, but
these holes were on 12 inch centers. The eight, upper cone
segments were joined together with bolts through their side
flanges. Once the eight segments of the upper cone section were
joined, the entire upper cone section was attached to the flange
welded to the cut line on the original cone. The lower cone
section (Dwg. 735 A-71356) was fabricated as a single section
with flanges on its top and bottom. The drawings called for both
flanges on the lower cone section also to have 13/16 inch
diameter bolt holes drilled on 6 inch centers. The lower cone
section was 5 feet high with a 9 feet 9 inch inside diameter on
the top and a 4 feet inside diameter on the bottom. The lower
cone section was installed as a single piece to the bottom of the
upper cone section. The hydraulic gate assembly attached to the
bottom of the lower cone section. The specifications on the
drawings called for all bolt connections to be made with A-325, 2
inch long, 3/4 inch diameter steel bolts.
1995 Cone Replacement
Jim Walter Resources decided in 1995, as they had in 1991, that
because of the wear on the cone section of the rock bin, it was
necessary to replace the cone. The drawing (735A-71355, 71356,
and 71357) prepared by Ira Lanstrum, which had been used for
fabrication and installation of the cone section in 1991, were
again used to fabricate and install the new cone section in 1995.
The entire upper cone section was replaced in 1995. The top
flange, which had in 1991 been welded to the original cone at the
cut line was not replaced in 1995. As in 1991, Professional Iron
Workers (PIW) was retained to install the newly fabricated cone
section. The new cone sections were fabricated in 1995 by Caine
Steel. The cone was replaced during the miner's vacation between
July 17 and July 22, 1995.
Deterioration of the Compression Ring
The compression ring beam transfers the majority of the load from
the weight of the refuse and rock within the bin and the self
weight of the cone out to the main structure of the refuse bin.
The compression ring beam consists of two 1/2 inch plates acting
as flanges and the sections of the 1/4 inch cylinder plate
between them, acting as the web. There were several locations
observed where the web of the compression ring was completely
corroded and/or worn through leaving large holes. In areas where
the metal had rusted through, permanent deflections of up to 1/2
inch were measured between the beam's two flanges. Severe
deterioration such as this affected the compression ring beamūs
ability to transfer loads from the cone to the main structure and
more importantly the characteristics of this load transfer would
have been altered. Large areas of deterioration of the web,
such as those observed, led to non-uniform stiffness within the
compression ring beam. This non-uniform stiffness resulted in
localized stress concentration in areas surrounding the
deterioration. These areas of concentrated stresses would likely
have lead to non-uniform stresses within upper connections of the
cone including the weld of the top flange to the cone at the cut
line and the bolted connections between this flange and the
flange on top of the upper cone section.
During the interviews, numerous witnesses stated that it was
known among the heavy equipment operators that an operator should
not get out of his equipment at the rock bin due to rocks falling
out of the cylinder on the north side. There were several
incidents reported of minor equipment damage due to falling rocks
and one incident of a miner being injured by a falling rock while
walking up the stairs on the north side of the bin. During the
interviews with management personnel, it was determined that they
were aware of the problems and had ordered material to repair the
holes in the cylinder. The material to repair the holes in the
cylinder wall arrived on mine property approximately two weeks
prior to the accident and preparations were being made for the
repair work to be conducted.
Inspection of the 1991 Connection of the Top Flange at the Cut Line
The original cone was specified to be cut along a line that was
approximately 7 5/16 inches below the attachment point of the
cone to the cylinder in 1991. Cut depth measurements taken
during the investigation varied from 7 to 9 inches around the
perimeter. The top flange was then welded to the original cone
at this cut line. Therefore, the top flange was approximately 13
1/2 inches above the bottom of the 21-inch deep beam making up
the octagon structure at level elevation 173 feet 3 inches. This
configuration left minimal space for welders to work when welding
the upper side of the top flange to the cut cone. There were
several areas where there would not have been sufficient room for
the welders to directly see this area as they were welding it
because their heads would not fit between the beam and the flange
while welding.
Another problem relative to this weld was that once the original
cone was cut, it is unlikely that the bottom of the cone section
would have been perfectly round. The cone would have been
subjected to many factors which over the preceding 14 years would
have left it deflected from its original circular shape at the
cut line level. These factors include the continual pounding
from rocks falling off the end of the belt and minor deflections
caused by the columns being impacted by equipment. Consequently,
the top flange, which had been rolled to fit a circular cone with
a straight cut line, would not have fit exactly against the cone.
Much of the weld between the top flange and the original cone
failed during the cone fall. There were many areas observed that
had minimal welds and a few areas that had no signs of a weld
between the top flange and the original cone. In many areas of
this flange connection, the weld material was uneven and non-
uniform. Furthermore, there were several places where a steel
bar had been placed between the top flange and the cut off cone.
The upper side of this bar had been welded to the original cone
and the lower side welded to the top flange. It appears obvious
that this was done because the gap between the top flange and the
original cone was too large to weld. This gap was further
evident in areas where weld material flowed completely behind the
gusset plates being welded to the cone because the flange and
gusset plate were not tight against the cone. This void between
the two metals affected the integrity of the weld.
This weld held the bin from the date the top flange was installed
in 1991 until the binūs failure in 1995. However, the weld
conditions described above would have created a situation where
this connection was stronger in some areas than others.
Particularly in the locations of the minimal welds and no welds,
stress concentrations would have been created in adjacent areas
where the weld was more competent.
Inspection of the 1995 Connection of the Upper Cone Section to 1991
Top Flange
In addition to the alignment problem resulting from attaching the
fabricated cone replacement section with its circular top to the
out of round existing cone, another misalignment was encountered
in 1995. The fabricating drawings prepared for the cone
modification made in 1991 and used again in 1995, called for the
bolt holes to be placed on 6 inch centers on all horizontal
flanges and 12 inch centers on the flanges running up the side of
the upper cone section. In 1991, the bolt holes were apparently
drilled on 6 1/2 inch centers on all of the horizontal flanges.
This discrepancy actually did not affect the installation of the
replacement cone in 1991 as the bolt holes in all of the
horizontal flanges were drilled on the 6 1/2 inch centers. The
bolt holes in both flanges were therefore aligned.
In 1995, the upper and lower cone sections were replaced, but the
1991 top flange welded to the original cone at the cut line, was
not. The 1995 replacement cone was fabricated according to the
specifications on the 1991 drawings, with bolt holes on 6 inch
centers. As a result, when the installation of the replacement
cone in 1995 was done, the bolt holes in the top flange and those
in the upper flange on the upper cone section did not align as
the bolt holes on the former were on 6 1/2 inch centers and on
the latter 6 inch centers. In order to connect these two
flanges, some existing bolt holes were enlarged and additional
bolt holes were made by burning. The result was odd shaped
holes, enlarged bolt holes, and unevenly spaced bolt holes. In
at least a couple of areas, there was severe misalignment of the
upper flanges causing the bolts through the upper cone section to
completely miss the top flange welded to the original cone
section. The result of these conditions was that fewer bolts
were installed than specified in the design.
Supplemental larger size gusset plates were added around the
perimeter of the cone at the eight support locations. These
plates were welded perpendicular between the cone and the webs of
the 21 inch deep beams in the octagon shaped frame. The welded
connection between the components appeared to be irregular and in
some locations the gusset plate did not meet flush with the cone.
Damaged Main Support Columns
The failure of the cone resulted in its impacting and damaging
various structural components on the bin frame as it was falling.
The walkway flooring and the channel support members at the level
of the hydraulic gate (drawing elevation 151 feet), were
completely destroyed by the falling cone. Three of the four main
W12x27, horizontal support beams for this floor level were also
damaged by the falling cone. The damage done by the falling cone
appeared to be limited to those areas at this level and several
bracing members below. There was damage to three of the four
main W10x49 columns, but most of this damage appeared to have
existed prior to the cone failure. The locations and alignment
of the permanent deflection in the columns suggested that this
damage was done by vehicular impact rather than by impact from
the falling cone. Bracing had been attached to the bent columns
before the bin failure. The post failure location of this
bracing was an indication that most of the damage to these
columns existed before the cone fell. Also, testimony by mine
personnel clearly indicated that the columns were damaged by
trucks running into them and that the southwest column was the
most severely damaged prior to the bin failure. The deflection
of the south west column was at a location 7 feet above its
foundation and was measured to be 9 1/8 inches off vertical
toward the west.
The elevations of the cross members supporting the cylinder were
surveyed by JWR personnel following the failure. The
measurements were taken at the four corners of the W21x55. The
south west corner was at least 0.85 inches higher than the other
corners. Since a survey was not conducted prior to the fall,
comparison could not be made between pre and post failure
elevations. Therefore, it was not clear whether this elevation
difference was the original as-built level, the result of the
truck impact on the columns, or the result of the cone impact on
the lower level.
Gate Impact
The possibility of gate impact by the bed of the truck was
investigated. The witness who viewed the cone fall stated that
the victim's truck bed was not extended and did not hit the gate.
The witness also reported that just prior to the accident he had
cleaned out accumulated material on the ground with his scraper
pan. To further investigate this possibility, a representative
from the crushed truck manufacturer inspected the condition of
the hydraulic hoses and the lift cylinders. The hoses were not
blown and the cylinders were removed for testing. If the bed had
been extended at the time of failure, presumably the hose would
have blown or the cylinder would have failed. Based on the
manufacturers findings, the bed was not extended when the cone
landed on the truck. The investigating team did not find any
markings on the side of the gate.
CONCLUSION
As previously mentioned, the location the cone cut off line
specified for the 1991 retrofit design left minimal clearance for
welding a flange plate to the original cone. The design also did
not clearly specify what type of welded connection should be made
at that interface. In addition to these design factors, the out-
of-round shape of the cone and the uneven cut line adversely
affected the quality of the weld that could be made between the
top flange plate and cone. The alignment problems were further
complicated when the flange installed in 1991 with predrilled
holes of 6 1/2 inch centers was joined to a cone section in the
1995 with holes drilled on 6 inch centers.
According to witness testimony, the conditions of the compression
ring and the top flange connection were not inspected when the
decision was made to replace the cone below the flange in 1995.
There also was no inspection of the construction during or after
the 1995 replacement.
Based on the evidence and the final position of the cone, it
appears that the failure initiated on the western side of the
structure and progressed toward the east before the cone dropped.
The failure occurred along the flange connection as the result of
an over-stressing of this area. The primary contributing factors
appeared to be missing bolts, oversized bolt holes, poor quality
welds between the original cone section and the 1991 upper flange
plate, and rusted holes above the compression flange. These
conditions caused the load to redistribute to the stiffer areas
where the connections were adequate. Ultimately, the load
redistribution over-stressed the connections along the western
side of the cone causing it to fall. The cone fell onto a truck,
resulting in the fatality of the operator who had pulled under
the refuse bin.
ENFORCEMENT ACTIONS
- A 103-K Order Number 3397387 was issued to ensure the safety of
miners until the investigation was completed.
- A 104-D-2 Order Number 3397782 was issued because the rock bin
structure was not being maintained in good repair to prevent
accidents and injuries to employees, a violation of 30 CFR,
Section 77.200.
Respectfully submitted by:
Walter W. Deason
Coal Mine Safety and Health Inspector
Donald T. Kirkwood
Civil Engineer
Terence M. Taylor
Civil Engineer
Approved by:
Michael Lawless
District Manager
Related Fatal Alert Bulletin: FAB95C40
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