UNITED STATES
DEPARTMENT OF LABOR
MINE SAFETY AND HEALTH ADMINISTRATION
District 2
Accident Investigation Report
(Surface Coal Mine)
FATAL HAULAGE
River Hill Coal Co. (I.D. No. 36 00884)
River Hill Coal Co., Inc.
Karthaus, Clearfield County, Pennsylvania
May 5, 1996
by
William D. Sparvieri, Jr.
Coal Mine Safety and Health Inspector
Michael M. Zenone
Coal Mine Safety and Health Inspector
Joseph F. Judeikis
Mechanical Engineer
Approval and Certification Center
John W. Fredland, Jr.
Civil Engineer
Pittsburgh Safety and Health Technology Center
George H. Gardner
Civil Engineer
Pittsburgh Safety and Health Technology Center
Originating Office - Mine Safety and Health Administration
New Stanton District Office
R.R. 1, Box 736, Hunker, Pennsylvania
Joseph J. Garcia, District Manager
GENERAL INFORMATION
The River Hill Coal Co. Mine, operated by River Hill Coal Co.,
Inc., is located 1.7 miles off State Route 879 at Karthaus,
Clearfield County, Pennsylvania. The mine consists of seven
active strip pits and a preparation plant. Employment is
provided for 109 persons. Coal is mined from the Upper and
Middle Kittanning and Moshannon coal seams, which have a combined
thickness of up to 75 inches. The mine operates two 12-hour
shifts a day, six days a week. Average production is 3,000 raw
tons of coal a day.
Overburden is drilled with highwall drills, shot, and removed
with a dragline, excavators, bulldozers, and rock trucks. Coal
is loaded into trucks with front-end loaders and transported to
the preparation plant for processing.
The principal officers at the mine are:
Harry C. Hancher..............President/Superintendent
John Fox...........................Safety Director
The last Mine Safety & Health Administration (MSHA) regular
Safety and Health inspection was completed on March 29, 1996.
DESCRIPTION OF ACCIDENT
On Saturday, May 4, 1996, the 004-0 pit crew, under the
supervision of William L. Moore, foreman/excavator operator,
started their shift at 6:00 p.m. The crewþs assignment was to
load overburden which had been previously drilled and blasted.
Upon arrival at the 004-0 pit, the crew conducted a pre-
operational inspection of the equipment.
At approximately 6:10 p.m., Moore began loading overburden. A
Caterpillar 5230 excavator was used to load the three Caterpillar
785B rock trucks used on this job site. Jack E. Gaines,
bulldozer operator, using his 2-way radio, suggested that one of
the trucks haul to the middle dump area and the other two trucks
haul to the lower dump area. Burton J. Fry, rock truck driver,
said that he would haul to the middle dump area. The work of
moving the overburden progressed with Fry hauling each of his
loads to the middle dump area while Timothy W. Gaines and Leonard
L. Martin, the other two rock-truck drivers, hauled most of their
loads to the lower dump. Timothy Gaines and Martin also hauled
an occasional load to the middle dump area while the lower dump
was being "pushed off" by the bulldozer.
At 12:01 a.m., May 5, 1996, Fry pulled along side the excavator,
had his truck loaded with rock and traveled to the middle dump.
At approximately 12:10 a.m., Timothy Gaines had just completed
dumping at the lower dump area and was parked facing the middle
dump. Timothy Gaines said that he could see the back-up lights
of Fry's truck as Fry backed towards the edge of the middle dump.
Moments later he saw the headlights facing downhill and the truck
sliding on the bed and cab down the side of the dump. Timothy
Gaines, using his two-way radio, notified the other miners of the
occurrence and started driving to the accident site. Moore and
Jack Gaines exited their equipment and ran to Fryþs truck.
The truck had come to a stop near an old haul road at the base of
the dump. The truck was back on its tires with the headlights
facing up the slope. Upon arrival at the rock truck, Moore
climbed up to the operator's cab to check Fryþs condition. When
Jack Gaines arrived, he was informed by Moore that Fry was not in
the truck. Jack Gaines began looking for Fry along the old haul
road. As Moore turned the truck engine off using the master
switch located near the front bumper, Jack Gaines found Fry
approximately 25 feet from the truck. Observing that he was
seriously injured, Jack Gaines told Timothy Gaines to call for an
ambulance while Moore, treating Fry for shock, placed a vest over
him. Timothy Gaines drove his rock truck to the parking area.
Using his personal pick-up truck, he drove approximately one mile
to a private residence to call Clearfield County 911 and report
the accident. Gaines then telephoned Joseph Potter, foreman, to
notify him of the accident. Potter, who was at home, traveled to
the mine immediately.
At 1:00 a.m., an ambulance with emergency medical technicians
from the Karthaus Ambulance Service arrived at Fry's location.
The victim was treated and taken to Philipsburg Hospital from
which he was transported by medical helicopter to Conemaugh
Hospital, Johnstown, PA. He died there of his injuries at 1:54
p.m., May 5, 1996. The cause of death was multiple skull
fractures and blunt force trauma.
PHYSICAL FACTORS INVOLVED
The investigation revealed the following factors relevant to the
occurrence of the accident:
- The weather on Saturday night May 4, 1996, and Sunday
morning May 5, 1996, was clear and dry, with the temperature
in the mid 40's.
- The overburden material being hauled from the 004-0 pit to
the middle rock dump consisted predominantly of relatively
clean shot rock.
- The top of the middle dump was relatively level and the
surface material was dry. An open area approximately 20
feet wide existed along the south edge of the dump where no
berm had been established. Overburden approximately 4 to 6
feet high had been deposited everywhere else on the
remaining edge of the dump to prevent overtravel. To the
left of the opening, large tire indentations were observed
in the berm material, almost the full height of the berm,
indicating that a haul truck had backed into it.
Rock-truck size tire tracks were observed to the edge of the
dump in the open area. The tire tracks did not indicate any
evidence of skidding before the overtravel occurred.
However, evidence was present to indicate that the truck had
been backed to the edge of the dump on a slight angle,
allowing the right rear tires to reach the edge before the
left rear tires. Along the edge where the truck went over
the dump, there was no indication that the truck had been
driven up on a berm and then had traveled over the edge.
Furthermore, there were no markings on the back or bottom of
the truck rear axle consistent with the truck having driven
through a berm. The ground clearance under the truck rear
axle is 32 inches.
After the accident, the condition of the edge of the pile
was consistent with the truck either rolling over the edge,
or backing to a point very close to the edge and going over
the edge when the edge gave way under the weight of the
truck. In the latter case, additional forces may have been
applied to the edge of the pile from the braking force of
the truck, and/or from the bed being raised.
- The distance from the top of the middle dump to the old haul
road was 150 feet. The slope angle of the rock dump varied
between 35 and 39 degrees.
- The truck involved was a 1993 Caterpillar Model 785B rock
truck, Serial No. 6HK00207. The hour meter indicated the
truck had been in service for 11,611 hours. The load
capacity of the 785B is rated at 102 cubic yards. The
maximum operating weight is approximately 550,000 lbs. (275
tons). The total empty weight is approximately 209,000 lbs.
(105 tons).
- The transmission selector lever (gear shift) was found in
the neutral position and the park brake switch was off.
There was no evidence to indicate the position of the truck
bed at the time the truck traveled over the edge of the
dump.
- The Caterpillar 785B rock truck was equipped with four
braking systems: Service, parking, retarder and secondary.
When any of the four braking systems was activated, both
front and rear brakes are engaged. The service, secondary
and retarder braking systems are oil cooled air over
hydraulic wet disc. The parking brake system is spring
applied, hydraulic release, utilizing the same disc packs as
the other three braking systems.
The thicknesses of both front brake disc packs were checked
and found to be in "as new" condition, indicated by no
measurable wear on the disc packs. The master cylinders for
both the front and rear brakes had not experienced any
overstroke. This indicates that the slack adjusters were at
the proper adjustment and the hydraulic side of the service,
secondary and retarder brake systems was at the proper
adjustment and functioning properly.
All four braking systems were tested from point of
activation down to the wheels. Drawbar pull tests were
conducted using a 0 to 100,000 lb. tension link. All four
individual braking systems met or exceeded the
manufacturerþs specifications. An external compressed air
source was connected to the truck and pressures were
measured on both the hydraulic and air sides of the brakes.
Upon actuation of the individual brake systems, all air and
hydraulic pressures were maintained within the
manufacturerþs specifications. The parking brake release
system was also checked and found to be operating properly.
- The Caterpillar 785B rock truck was equipped with a
transmission neutralizer switch. The transmission
neutralizer switch is an electrical interlock which
automatically shifts the transmission from reverse to
neutral when an attempt is made to raise the bed while the
transmission is in reverse. The transmission neutralizer
switch was checked and found to be correctly operating as
designed. The bed raise/lower lever linkage was also
checked. Although the lever was out of adjustment 2.9
inches, the lever, lever linkage and transmission
neutralizer switch were all operating properly.
The rock truck was equipped with a six speed wet clutch
automatic transmission. In order to test the transmission,
an auxiliary hydraulic power supply, which provided
approximately 20 gallons per minute at 400 psi, was plumbed
directly into the transmission where the hydraulic supply
and return lines were normally connected. This allowed the
rotary selector spool and the clutches to be checked without
the truckþs engine running.
The transmission was evaluated in four positions: Neutral 1,
neutral 2, reverse and first gear. The evaluation consisted
of determining the proper operation of the following:
- Transmission selector lever
- Transmission neutralizer switch
- Transmission rotary selector spool
- Transmission gear indicator
- Clutch pressure for clutches Nos. 1 and 6 at the
corresponding pressure tap points labeled B and G.
The evaluation was made to determine if the transmission
would shift out of reverse gear when either the body raise
switch activated or the transmission selector lever was
moved from reverse to neutral. Test results indicated that
all associated switches, components, valves, solenoids and
clutches were working properly.
- Both steering accumulators were checked for their nitrogen
charge. The manufacturer specifies approximately 1,200 psi
as the correct nitrogen charge. The results of the tests
were:
- Right side accumulator 780 psi
- Left side accumulator 700 psi
The accumulators were checked with 0 psi pressure on the
hydraulic side in order to obtain a true measure of the
accumulator nitrogen charge pressures. Although the
steering accumulators were not charged up to the
manufacturer's specifications, they did contain a magnitude
of reserve. This reserve would provide hydraulic dampening
of the steering system under normal operation and also
provide auxiliary assist to steering in the event of engine
failure.
- The Caterpillar 785B rock truck was equipped with a Payload
Measurement System (PMS) and an Electronic Monitoring System
(EMS). Computer printouts obtained from the PMS revealed
the following information:
- The truck was hauling the 23rd load for the shift.
- The truck was loaded with the final load at 12:01 a.m.,
May 5, 1996.
- Travel time from the pit to the dump site for the 23rd
load was 2.87 minutes, with a load of 155.8 tons.
- During the previous 22 loads, the truck hauled between
146.3 tons and 167.1 tons per load.
The EMS monitors and records certain aspects of engine and
transmission operation, and records events occurring outside
the manufacturer's established operating parameters. A
review of the data provided by the EMS did not identify any
fault codes that may have played a role in the cause of the
accident.
- A seat belt provided in the operatorþs compartment was found
intact and not buckled. Rollover protection was provided
and the operatorþs cab sustained very minor damage.
- William Moore received first-aid training and treated the
victim for shock until the ambulance arrived.
- A review of the Karthaus Ambulance Service's log book
indicated that 28 minutes had elapsed between the time of
the accident and the time the ambulance service was
notified. This was due to the fact that emergency
communications were not provided at the mine site. River
Hill Coal Co. Inc., provides five cellular telephones in
company vehicles, however the persons assigned these
vehicles were not scheduled to work the 6:00 p.m. shift on
May 4, 1996. Therefore, the vehicles with the phones were
not on mine property at the time of the accident.
CONCLUSION
The accident occurred because overburden was being dumped at the
edge of the middle dump where an adequate berm was not in place.
The lack of a berm allowed the truck to either overtravel the
edge of the dump, or get close enough to the edge that the edge
gave way under the rear tires. The not wearing of the seat belt
contributed to the severity of the injuries.
ENFORCEMENT ACTIONS
- A 103(k) order was issued to ensure the safety of miners
until an investigation into the cause would be completed.
- An adequate berm or similar means to prevent overtravel was
not provided at the middle rock dump, a violation of 30 CFR,
77.1605(l).
- The operator of the Caterpillar 785B rock truck was not
wearing the seat belt provided. The truck was equipped with
rollover protection, a violation of 30 CFR, 77.1710(I).
- Emergency communications were not provided for the 004-0
pit, a violation of 30 CFR, 77.1701(a).
Respectfully Submitted by
William D. Sparvieri, Jr.
Michael M. Zenone
Joseph F. Judeikis
John W. Fredland, Jr.
Approved by:
Joseph J. Garcia
District Manager--Coal Mine
Safety and Health District 2
Related Fatal Alert Bulletin: FAB96C16
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