UNITED STATES
DEPARTMENT OF LABOR
MINE SAFETY AND HEALTH ADMINISTRATION
OFFICE OF THE ADMINISTRATOR
COAL MINE SAFETY AND HEALTH
REPORT OF INVESTIGATION
UNDERGROUND COAL MINE BURST
(RIB FALL)
C-2 MINE - I.D. NO. 15-07201
HARLAN CUMBERLAND COAL COMPANY
DIONE, HARLAN COUNTY, KENTUCKY
NOVEMBER 20, 1996
by
Billy G. Foutch
Supervisory Coal Mine Safety and Health Specialist, Norton, VA
Charles H. Grace
Conference and Litigation Representative, Barbourville, KY
Curtiss Vance
Coal Mine Safety and Health Inspector, Logan, WV
Michael A. Evanto
Pittsburgh Safety and Health Technology Center
Geologist, Pittsburgh, PA
George J. Karabin, Jr.
Pittsburgh Safety and Health Technology Center
Supervisory Civil Engineer, Pittsburgh, PA
Danny Harmon
Supervisory Coal Mine Safety and Health Specialist
(Roof Control), Pikeville, KY
Originating Office - Mine Safety and Health Administration
Office of the Administrator - Coal Mine Safety and Health
4015 Wilson Boulevard, Arlington, Virginia 22203
Marvin W. Nichols, Jr., Administrator
Release Date: April 14, 1997
OVERVIEW
Abstract of Coal Burst
At approximately 2:08 p.m. on November 20, 1996, a coal burst
occurred on the 005-0 working section located in the Second Left
panel off Nine Right off of the No. 3 East Main entries of
Harlan Cumberland Coal Company's, C-2 Mine. Nine miners were
working on the section at the time of the burst. The coal burst
resulted in the deaths of two of the miners located on the
section. Four other miners sustained varying degrees of injury.
As room pillar No.1 was mined, much of its load was released and
transferred to the already highly stressed adjacent pillars.
This sudden pressure increase on the adjacent pillars was
sufficient to cause failure of coal near or into the core of
these pillars, and resulted in the burst.
The coal ribs were not controlled to protect persons from the
hazards of a coal burst in the three rooms off Second Left (MMU
005-0), an active working section where persons worked and
traveled. The coal burst damaged the ribs of all nine pillars
in the rooms, blowing in excess of 1,500 tons of coal into the
room entries and crosscuts.
Background
The Harlan Cumberland Coal Company, C-2 Mine located near Dione,
Harlan County, Kentucky, began operation on or about October 1,
1980. The mine is developed and serviced through three portals
consisting of drift openings into the Creech Coal Seam. The
coal seam ranges in thickness from 42 to 96 inches.
The principal management officers of the mine at the time of the
coal burst were:
Joe T. Bennett.........................................President
C. V. Bennett III.....................................Vice-President
Catherine Bennett McCue.......................Secretary
Clyde V. Bennett....................................General Manager
The coal mineral rights are owned by Catherine Bennett McCue,
Karen Bennett Loving, Joseph T. Bennett, Darby Bennett, and the
Cornett-Lewis Estate and are leased to Harlan Cumberland Coal
Company. Owners of the surface area are Ark Land Company and
Nally & Hamilton.
The mine employs a total of 55 miners and produces coal two
shifts per day, six days per week. Equipment maintenance is
performed on a separate nonproducing shift.
The mine is a two unit mine with one advancing and one
retreating unit. The advancing 004-0 section utilizes a five
entry system. The retreating 005-0 section utilizes a five
entry system and develops rooms to the right of the panel
entries. Room pillars are extracted first, followed by the
adjacent entry pillars.
At the time of the coal burst, eight miners and a foreman were
working underground on the 005-0 working section. The section
had completed development of a set of three rooms and was in the
process of extracting the No. 1 room pillar.
The mining system on the 005-0 working section utilized a Joy
14CM Continuous Mining Machine, two Joy 10SC Shuttle Cars, an
Elkhorn AR-95 Battery-Powered Scoop, and a Fletcher Twin Boom
Roof Bolting Machine with "T-Bar" Automated Temporary Roof
Support System (ATRS).
A MSHA regular Safety and Health inspection (AAA) was ongoing at
the time of the accident. The previous inspection (AAA) was
completed on September 24, 1996.
THE COAL BURST
On Wednesday, November 20, 1996 at approximately 5:45 a.m., the
005-0 working section's second (day) shift crew, consisting of
eight miners traveled underground accompanied by Darrell Lewis,
foreman. Arriving on the section at approximately 6:25 a.m.,
they were met by Ernie Boggs, maintenance foreman, who had
conducted the pre-shift examination earlier that morning. Boggs
reported to Lewis that nothing unusual had been found during the
course of his examination.
Darrell Lewis proceeded to issue instructions to the crew
members and coal production began at approximately 6:30 a.m.
Production commenced by advancing the left crosscut in the No. 2
room. Successive cuts were then advanced without incident, in
all three rooms, until the room entries and crosscuts were
connected to the gob.
After completing these connections the continuous mining machine
was moved to the No. 1 room pillar to take the initial cut,
beginning pillar extraction. The initial cut was advanced into
the No. 1 pillar approximately 15 feet deep when, at
approximately 2:08 p.m., a coal burst occurred, claiming the
lives of Mark Skidmore and, subsequently, that of Randy Lewis,
both roof bolting machine operators. Four other miners
sustained various degrees of injury. Injured were: Darrell
Lewis; John Carroll, scoop operator/roof bolting machine
operator; and, Jim Carr and David Harris, both continuous mining
machine operators.
The force of the coal burst was felt by other employees located
on the 005-0 working section and was detected by seismic
stations of the University of Kentucky, at four locations,
averaging a magnitude of 2.7 on the Richter Scale. However, no
persons outside the immediate area of the coal burst were
adversely affected. No other significant seismic events were
recorded either immediately prior to or after the accident.
RECOVERY OPERATIONS
At approximately 2:25 p.m., Kenneth Fee, MSHA, Harlan, Kentucky
Field Office Supervisor was notified of the accident by Clyde V.
Bennett of Harlan Cumberland Coal Company. Bennett reported
that a "bump" had occurred on the 9 Right unit at the C-2 mine
and that at least one miner was unaccounted for.
Fee immediately dispatched inspectors from the Harlan Field
Office, accompanied by Robert W. Rhea, MSHA Field Office
Supervisor, to the mine site. Fee next notified John M. Pyles,
Assistant District Manager, of the accident.
MSHA inspectors arrived at the site at approximately 2:55 p.m.
Upon their arrival, the inspectors were met by state inspectors
led by Ronnie Hampton of the Kentucky Department of Mines and
Minerals and Johnny Smith, outside person, for the C-2 mine.
Smith briefed Rhea, essentially providing the same information
as Bennett had provided earlier to Fee. Smith identified the
unaccounted-for miner as Mark Skidmore, Roof Bolting Machine
Operator.
Rhea and Hampton assembled a recovery team consisting of MSHA
and state inspectors and Eddie Sargent, Safety Director for
Harlan Cumberland Coal Company, who had just arrived at the
mine. The team then entered the mine while Rhea remained on the
surface to coordinate recovery efforts. At that time, Matthew
Coots, 004-0 Section Foreman, called to the surface and informed
Rhea that two of the injured miners were en route to the surface
and that Skidmore remained unaccounted for. Rhea continued to
coordinate recovery efforts until the arrival of John Pyles at
4:30 p.m. Pyles was accompanied by Charles Grace, MSHA
Conference and Litigation Representative. Coordination of
recovery efforts were turned over to Pyles as the senior MSHA
official on site. Rhea then traveled underground to assist in
recovery efforts.
The recovery team arrived on the 005-0 working section where
they encountered Ron Painter, shuttle car operator, at the 005-0
section feeder. Coots and Louis Blevins, Superintendent,
assisted by six other miners, were in the process of moving the
coal, rock, and debris which resulted from the burst.
Additional roof support material, including cribbing, was then
brought up to that position. Larry Bush, Federal Inspector,
then proceeded to re-establish ventilation to the area where
ventilation controls (curtains) in the face area had been
dislodged by the burst. The recovery team proceeded steadily,
installing roof support and removing the loose coal and rock in
the area of Skidmore's last known location.
Skidmore's body was discovered at approximately 9:45 p.m.,
recovered, and was transported to the surface by battery powered
personnel carrier, arriving at the portal at approximately 10:30
p.m. Skidmore was formally pronounced dead by Deputy Harlan
County Coroner, Gerald Scott at 10:45 p.m.
INVESTIGATION OF THE COAL BURST
MSHA and the Kentucky Department of Mines and Minerals (KDMM)
cooperated to conduct a joint investigation. Billy G. Foutch
was appointed as leader of MSHA's investigation team. The
primary focus of the investigation was to determine the cause(s)
and extent of the burst and to assess the nature of geologic
conditions in the area.
MSHA personnel from the Harlan and Barbourville, Kentucky
offices provided information in regard to mine conditions,
practices, and plan requirements. A pre-investigation
conference and briefing was held at MSHA's Harlan Field Office
on November 21, 1996. During this conference, mine and accident
information was principally provided by Joseph W. Pavlovich,
MSHA District Manager, and by John M. Pyles, to the joint
investigation team and Kathy Snyder, representing MSHA's Office
Information and Public Affairs. The C-2 mine employees did not
designate a representative of the miners to participate in the
investigation.
The on-site investigation began on November 21, 1996. On the
first day of the investigation, mine records were examined in
order to determine pre-existing conditions and practices. The
underground examination of the accident scene was delayed due to
ventilation problems and the presence of methane discovered
earlier by inspectors of MSHA's Harlan Field Office and concerns
for safety of the investigation team.
The next morning, on November 22, 1996, with the ventilation
problems corrected and with methane and oxygen at acceptable
levels, the joint investigation team entered the mine
accompanied by company personnel. The accident investigation
was organized with personnel assigned: to map the accident area;
to evaluate the roof control system and conditions; to assess
geologic conditions; to determine the extent and magnitude of
the coal burst; and to photograph and collect information. In
addition, roof conditions and roof control practices in other
areas of the mine were evaluated in order to determine any
correlation to similar conditions and practices which may have
existed on the 005-0 working section prior to the accident. The
005-0 section ground conditions continued to deteriorate after
the accident and the scene was essentially found covered by
coal, rock, and debris to the extent a full assessment and
examination of the area was impractical. The investigative
assignments were completed within several hours, and the
investigators exited the Related Fatal Alert Bulletine investigation, MSHA and KDMM conducted
interviews of persons with knowledge of the facts and
circumstances surrounding the coal burst. Interviews were
conducted with individuals between December 2, 1996 and December
13, 1996. Twenty-four interviews were conducted at the MSHA
Field Office in Harlan, Kentucky, and one interview was
conducted at the home of a seriously injured miner. The hourly
employees did not designate personal representatives during the
interviews. However, all officials and agents of Harlan
Cumberland Coal Company, including the mine engineer and survey
crew personnel, were represented by attorneys.
DISCUSSION
Mine Development and Roof Control History
The C-2 mine was developed from the surface in 1980. The mine
is served by three portals consisting of drift openings into the
Creech coal seam. The present workings consist of: two active
working sections, mains, panels, and an extensive gob consisting
of pillared-out workings and bleeder entries. The investigators
studied the history of roof control incidents at the C-2 mine.
Following is a discussion of four significant events that
occurred prior to November 20, 1996.
On January 11, 1990, a non-injury coal burst occurred on the
Second Right off No. 2 East Mains during pillar recovery
operations. The mine roof consisted of up to 10 feet of firm,
sandy shale followed by 10 feet or more of firm sandstone. The
mine floor was composed of firm shale that had heaved
substantially at some locations. Mining height was about 6.7
feet and the total overburden in the area was approximately 1300
feet. Coal pillars across the section had generally been
developed to dimensions of approximately 40 feet by 60 feet.
The burst did not result in injury or damage to equipment.
However, the burst caused extensive damage to a large pillar (60
feet by roughly 175 feet in size) located adjacent to a block
being split and between one of the section's panel entries and
the old workings of the East Main headings. Moderate damage was
sustained by another adjacent pillar. Subsequent to the burst
mining operations ceased at this location and mining resumed
approximately 300 feet outby the affected area. The burst was
investigated by MSHA and was found to have occurred as a direct
result of utilizing faulty mining methods that created a coal
pillar with dimensions not compatible with the effective control
of coal bursts.
In July, 1994, a "squeeze" condition occurred during pillaring
on the 8 Right section. The five entry panel had been developed
on 80-foot by 80-foot centers. Sets of five rooms were driven
to the right, on 80-foot by 65- to 75-foot centers, through a
340-foot wide barrier pillar separating the 8 Right and 7 Right
sections. After recovering approximately eight rows of blocks
the squeeze occurred, primarily in the newly developed rooms
outby the pillar line. Observations by MSHA's Pittsburgh Safety
and Health Technology Center (PSHTC) and District 7 personnel
revealed that the floor had heaved extensively with heavy pillar
sloughing, and several roof falls were noted toward the gob.
Mining height in the area was about six feet and overburden had
increased from less than 1,000 feet near the southern end of 8
Right to over 1,400 feet at the face. A borehole, located about
500 feet from the pillar line, disclosed the presence of massive
sandstone 22 feet above and six feet below the Creech seam, and
indicated the existence of a coal seam (six inches thick)
roughly six inches below the shale mine floor. This combination
of geological conditions may have contributed to the squeeze.
As a result of this evaluation, PSHTC made recommendations
including the design of barrier pillars and the reduction of
entry and crosscut widths to enhance pillar line conditions
during the retreat mining of the 9 Right and the proposed 10
Right sections.
Subsequent to the receipt of MSHA's Technical Evaluation, on
November 10, 1994, MSHA's District 7 Manager, Joseph W.
Pavlovich, forwarded a letter to the mine operator. The letter
instructed the operator that before pillar mining in 8 Right was
resumed following the "squeeze", that a revision to the approved
roof control plan would be necessary. The proposed revision was
to address MSHA's concerns as related in PSHTC's Technical
Evaluation of November 7, 1994, which was included as an
attachment to the letter.
On January 3, 1995, the mine operator responded to the District
Manager's request, providing a written plan in regard to
pillaring on the 8 Right Section. An investigation of the
operator's proposal was made by representatives of MSHA's Harlan
Field and District Offices.
On January 20, 1995, the District Manager denied approval of the
operator's proposal stating that the stress encountered would
not likely be relieved by mining the 8 Right pillars. Failing
to leave a barrier between 8 Right and 9 Right would continue to
cause overriding stress into the future panels. The operator
was asked to provide additional and clarifying information and
to resubmit the proposal.
During this period, the mine operator engaged the services of
three mining/roof control consultants; Dr. Kot F. Unrug of
Lexington, Kentucky, Henry L. Kiser of Abingdon, Virginia, and
Dr. David A. Newman of Appalachian Mining and Engineering, Inc.
of Lexington, Kentucky.
Two of the three consultants recommended leaving a barrier
pillar or additional pillars between 8 Right and 9 Right,
consistent with MSHA's previous recommendation. No further
pillaring was performed on 8 Right and the operator developed 9
Right, generally incorporating the consultants' recommendations
into the pillar and barrier design. A barrier pillar
approximately 330 feet in width was left between the 8 Right and
9 Right panels.
During the period of May through July, 1996, a severe loading
condition was experienced on the 1st Left off 3 East Mains
resulting in the abandonment of 29 pillars that had been planned
to be recovered. The 1st Left section was developed on 80-foot
by 80-foot centers as were panels and rooms to the right. After
retreating pillars successfully for about 2,200 feet,
deteriorating roof conditions, including numerous roof falls,
were experienced in the 1st Left and adjacent panels. While the
specific roof and floor composition is not known, mining height
averaged six feet, and cover steadily increased from less than
300 feet at the northern end of the 1st Left off 3 East Mains
panel to over 1,400 feet at the center of the affected area.
However, no problems were reported during pillar extraction in
outby areas where cover ranged from 1,380 feet to 1,200 feet.
In September of 1996, an event occurred during pillar recovery
on the 1st Left off 9 Right Section that caused that section to
be abandoned. The event has been described by various mine
personnel as a "pressure point" resulting in unstable roof, a
"squeeze" or a "bump". The area was primarily developed on 80-foot by 80-foot centers (60-foot by 60-foot pillars). However,
the pillars being extracted ranged from 50-foot by 60-foot to
60-foot by 60-foot in size. In addition, several pillars with
dimensions of 40 feet by 60 feet were located just outby the
blocks being mined when the event occurred. Reportedly, the
event occurred during the initial cut of a pillar (three pillars
had been cut in this manner) that affected it and an adjacent
block. This resulted in roof/floor convergence that temporarily
wedged a shuttle car in place and caused the subsequent
occurrence of a number of roof falls in the area. From a
borehole, located about 600 feet from the pillar line, the
immediate roof consists of 14 feet of dark gray shale that is
overlain by a 24-foot thick layer of massive sandstone. The
mine floor is composed of 1 foot of firm shale followed by 32
feet of massive sandstone. Mining height averaged 6.1 feet in
the area and cover varied from about 600 feet at the southern
end of the 1st Left off 9 Right panel to nearly 1,100 feet at
the face. Following the event, mining ceased and the section
was abandoned.
Roof Control Plan
The Roof Control Plan which was in effect at the time of the
accident was originally approved on June 2, 1995. The plan, as
was further revised on December 6, 1995, provided for full
overhead support in all advancing roof spans. Roof support on
the retreating 005-0 section is maintained with full overhead
support in the initial cuts of the pillar splits and posts in
the remaining split and lift cuts.
The roof control plan stipulated a maximum entry width of 20
feet, developed with a minimum distance of 60 feet between the
centers of entries and crosscuts and 50 feet between the centers
of rooms and crosscuts. The minimum pillar size for pillar
extraction is 40 feet by 40 feet.
Rods, fully grouted with polyester resin are used on the
advancing sections. The minimum length of the rods is 42 inches
with installation on 48-inch centers. Mechanically anchored,
tensioned roof bolts are used on the retreating 005-0 section.
The minimum length of the bolts is 30 inches installed on 48-
inch centers.
Mining Method and Roof Control (005-0 Section)
The 005-0 section (2nd Left off 9 Right) had been advanced as a
five entry panel on 80-foot by 80-foot centers to the property
boundary leaving minimum size coal pillars of 60-foot by 60-foot
in dimension. Entries were mined approximately 19 feet wide and
a barrier pillar, 230 feet in width, separated the panel from
the previously mined 1st Left panel off 9 Right. The roof was
supported with 4-foot long fully grouted bolts installed on a 4-foot by 4-foot pattern. Steel straps and longer bolts were used
as supplements where conditions warrant. The section was in the
process of retreating, recovering panel pillars. Mining on the
section also included the development of rooms into the adjacent
barrier pillar and the recovery of the room pillars. The burst
occurred during the recovery of the room pillars.
The normal retreat mining method used on the 005-0 section was
to develop five rooms on 80-foot centers through the barrier
pillar, with two rows of crosscuts turned on 90-foot and 80-foot
centers, respectively. Two rows of four pillars (in the
developed barrier) were then extracted from left to right,
followed by four rows of five pillars (four panel pillars and
the remaining barrier pillar) recovered from right to left.
At the accident location, the method of developing rooms in the
barrier pillar was changed from a five-room system to a three-room system. According to mine personnel, pressure on the
blocks had been increasing and it was hoped that by driving
fewer rooms, the pillars could be mined faster and more complete
caving would occur and relieve the pressure. It should be noted
that cover had increased to about 1,400 feet in this area and
the extent of the frontal gob had grown to nearly 1,000 feet.
The side gob, however, had been reduced to about 130 feet
adjacent to the face due to the boundary of the mine property.
General Mine Geology
The mine is located in the Creech coal seam. Mining height
varies from 42 inches to 96 inches. The immediate roof normally
consists of 10 feet to 18 feet of firm, sandy shale and the main
roof consists of 10 feet or more of firm sandstone. The
remaining overburden contains roughly 52 percent sandstone
(including a number of massive layers), 42 percent shale, four
percent siltstone and 2 percent coal. The mine floor is
composed of zero to three feet of shale followed by a massive
sandstone layer, usually in excess of 30 feet thick.
A number of coal seams exist above and below the Creech seam,
including the Harlan seam (about 375 feet below), the Darby seam
(roughly 150 feet below) and the High Splint seam (approximately
1,000 feet above). Mining in the Harlan seam has been confined
to areas east of the 7 Right section and north of the C-2
property. The Darby seam has been mined under the western
extent of the C-2 property and east of the 7 Right section. The
High Splint seam has also been extensively mined, but like the
Harlan and Darby seams, no mining over the active works of the
C-2 mine is known.
Overburden above the C-2 mine varies in the mountainous terrain
from under 100 feet near the drift mouth to over 1,600 feet at
the deepest point under Black mountain.
General Geology of the 005-0 Section
The immediate roof on the 005-0 section is composed of roughly
14 feet of firm dark grey shale as learned from a borehole
located 500 feet from the face. That same borehole indicates
the presence of a 36.8-foot thick massive sandstone layer and a
23.8-foot thick bedded sandstone formation immediately above the
shale roof. Additional sandstone layers 18.2, 7.1, 33.3, and
21.9 foot thick exist within the next 150 feet of overburden.
The mine floor consists of about 1 foot of firm shale followed
by 31.6 feet of massive sandstone.
Cover over the 005-0 section increased from less than 850 feet
at the eastern end of the panel to over 1,420 feet at the
accident site. Mining height averaged about 6.7 feet in the
vicinity of the accident site.
Ground Conditions On the 005-0 Section Prior to the Burst
Prior to the accident, conditions on the 005-0 section were
thought to be "normal" by the section crew. The gob was tight
around the perimeter of the section, the roof appeared stable.
Test holes drilled earlier in the shift and the previous shift
reportedly disclosed no cracks. According to the miners
interviewed, pillar sloughing was pronounced in some areas but
no red dust or signs of abnormal pressure were evident.
However, several miners did note that the roof bumped (cracked)
several times while turning the last crosscut in the No. 1 room
and that considerable roof bumping occurred in the vicinity of
the No. 1 room pillar as the initial cut began.
Description and Extent of the Burst
The coal burst on the 005-0 section occurred as the initial cut
was advanced about 15 feet into the No. 1 pillar of the No. 1
room. The burst resulted in damage to the ribs of all nine room
pillars, over 1,500 tons of coal blown into the rooms and room
crosscuts, injuries to four miners, and the death of two miners.
The extent of the burst is illustrated in the sketch labeled
"Accident Site Details - 005-0 Section" included in the front of
this report. The sketch was compiled from observations made on
November 22, 1996 and interviews with eyewitnesses to the event.
The No's. 2 and 3 pillars displayed the most damage as the gob
side ribs of these blocks (diagonally) were largely destroyed.
Blown coal was roofed at the back end of the No. 2 room and was
three to four feet deep inby the last open crosscut in the No's.
1 and 3 rooms. Blown coal was observed to the top (four feet
deep) of the roof bolting machine in the No. 2 room just outby
the last open crosscut. Blown coal was observed up to three
feet deep in the other affected areas. A fine red or rust
colored dust was present in all of the locations where coal was
blown into the rooms and room crosscuts.
Roof deterioration accompanied the burst at several locations,
further illustrating the violence of the event. Six inches to
two feet of roof rock fell from around the roof bolts and straps
in the No. 2 room. Timbers set at the mouth of the last open
crosscut between the No's. 1 and 2 rooms were broken and the
roof in that area was damaged. A heavy roof area developed in
the No. 2 room starting at the second crosscut outby the gob and
extended further outby through the opposite crosscut of the 2nd
Left panel to the No. 3 entry of the 2nd Left panel. In
addition, virtually all of the test holes in the No. 1 room and
the last open crosscut of the rooms, contained cracks at depths
ranging from 39 to 78 inches into the roof. These test holes
were drilled during the advance mining cycle and reportedly were
unfractured prior to the burst.
Roof conditions appeared stable over the remainder of the 005-0
section although occasional sounds, indicative of fracturing
high in the roof strata, were heard by investigators on November
22, 1996. Pillar sloughing became progressively less severe
away from the pillar line and burst area and was reduced to
corner spalling in the 2nd Left panel, 1 to 2 crosscuts outby
the gob end of the coal barrier. No floor heave was noted on
the 005-0 section, but blown coal in the rooms and crosscuts
prevented a thorough examination of bottom conditions in the
burst area.
SUMMARY AND CONCLUSION
Cause of the Accident
The investigation team concluded that the increasing size of the
frontal gob, the existence of a side gob, and increasing depth
of overburden (in excess of 1,400 feet), resulted in high
stresses and pressures on the coal pillars as they were
extracted. The side gob had narrowed to approximately 130 feet
wide adjacent to the accident site. The narrowness of the side
gob may have restricted caving, contributing to excessive
loading of the pillar line.
The presence of thick sandstone layers above and below the
Creech coal seam enhanced the ability of the coal pillars to
withstand high stresses and store energy. As room pillar No.1
was mined, much of its load was released and transferred to the
already highly stressed adjacent pillars. This sudden pressure
increase on the adjacent pillars was sufficient to cause failure
of coal near or into the core of these pillars, and resulted in
the burst.
The failure of the mine operator to fully address the above
factors and direct adjustments sufficient to control the high
ground pressures experienced by the active working section also
contributed to the cause of the accident.
CONTRIBUTORY VIOLATION
30 CFR 75.202(a)
The coal ribs were not controlled to protect persons from the
hazards of a coal burst in the three rooms in Second Left (MMU
005-0) off the Nine Right Panel, an active working section where
persons worked and traveled. On November 20, 1996, retreat
mining was started in the rooms and as the initial cut of coal
was taken from the middle of the No. 1 pillar block, a coal
burst was triggered. The coal burst damaged the coal ribs of
all nine pillars in the rooms, blowing in excess of 1,500 tons
coal into the room entries and crosscuts. The blown coal
injured six miners, two fatally.
The potential for a coal burst was known to the mine operator,
especially when mining beneath areas of high ground cover. The
mine operator had made some adjustments to the numbers of and
size of the pillars in the rooms in the Second Left section,
however the adjustments were not sufficient to control the high
ground pressures experienced by the active working section
before the coal burst occurred.
Respectfully submitted
Billy G. Foutch
Supervisory Coal Mine Safety and Health Specialist
Charles H. Grace
Conference and Litigation Representative
Curtiss Vance
Coal Mine Inspector
Michael A. Evanto
Geologist
George J. Karabin, Jr.
Supervisory Civil Engineer
Danny Harmon
Supervisory Coal Mine Safety and Health Specialist (Roof Contorl)
Approved by:
Marvin W. Nichols, Jr.
Administrator
for Coal Mine Safety and Health
Related Fatal Alert Bulletin: FAB96C34
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