UNITED STATES
DEPARTMENT OF LABOR
MINE SAFETY AND HEALTH ADMINISTRATION
Western District
Metal and Nonmetal Mine Safety and Health
Accident Investigation Report
Underground Gold Mine
Fatal Hand Tool Accident
Tonto Drilling Services Inc.
Contractor ID IU3
at
Meikel Mine
ID No. 26-02246
Barrick Goldstrike Mines
Carlin, Elko County, Nevada
March 9, 1996
By
Michael J. Drussel
Mine Safety and Health Inspector
Mine Safety and Health Administration
3333 Vaca Valley Parkway, Suite 600
Vacaville, CA 95688
Fred M. Hansen
District Manager
GENERAL INFORMATION
Donald Moore, diamond driller, age 42, was seriously injured
at approximately 12:15 p.m., on March 9, 1996, when he was
struck by a pipe wrench he was using to free core drill rods.
He died of his injuries on April 14, 1996. Moore had five
years of mining experience, all as a diamond driller with the
same company. Moore had received training in accordance with
30 CFR Part 48.
MSHA was notified at 1:30 p.m. on the day of the accident by
a telephone call from Charles Warner, loss control director
for the mining company. At the time it did not appear that
the injury was life threatening. An investigation was begun
on March 18 after MSHA was informed that Moore's condition
had worsened.
The Meikle Mine, an underground gold operation, owned and
operated by Barrick Goldstrike Mines, was located 28 miles
north of Carlin, Elko County, Nevada. The senior company
official was Roderick Pye, manager. The mine was under
development and was normally operated three 8-hour shifts a
day, five days a week. A total of 95 persons was employed.
As a part of the mine development, a production shaft and a
ventilation shaft had been sunk and about 3000 feet of drifts
were completed on three levels.
Tonto Drilling Services, Inc., headquartered in Salt Lake
City, Utah, was an independent core drilling contractor
enlisted to perform exploratory drilling on the 1225 level.
The firm specialized in this type work and had completed
similar jobs at other operations. The senior official at
this site was Daniel Mayberry, job superintendent.
Exploratory drilling was normally performed two 8-hour shifts
a day, five days a week. A total of 9 persons was assigned
to this job.
The last regular inspection of this operation was completed
on November 2, 1995. Another inspection was conducted in
conjunction with this investigation.
PHYSICAL FACTORS INVOLVED
The drill being used at the time of the accident was a Hagby
Model 1000. It was set up in the 1225(ramp) drill station
at a 18-degree down hole. The hole was collared about 24
inches above the sill of the station. A 400 foot string of
ten-foot NQ drill rods was stuck in the hole at the bit. NQ
is a designation for rods having a 2.75 inch outside
diameter.
Drill rods stuck in the hole was an occasional ocurrence.
Stuck rods were usually the result of the drill bit becoming
jammed between cracks or crevices, or the drill running dry.
When this occurred, it was routine practice to first apply
torque to the rods with the drill. If this failed to free
the bit, pipe wrenches were used to rotate the rods by hand.
The alternative was to reverse the rotation of the string of
rods, causing it to separate at one of the joints. Remaining
rods and the bit would then be abandoned.
The two Rigid (brand name)24-inch pipe wrenches involved were
of cast steel construction. The movable and stationary jaws
on both wrenches were in good condition with little wear. A
six-foot extension pipe commonly known as a "cheater" was
placed over the handle of one of the wrenches to increase
leverage. The use of a cheater pipe is not recommended by
the manufacturer in that the extra leverage can distort the
wrench and cause torque to be exerted in excess of the
wrench's design capacity. The pipe can also slip off the
handle causing the wrench to spring back forcefully.
DESCRIPTION OF ACCIDENT
On the day of the accident, Donald Moore (victim) began work
at 8:00 a.m., his regular starting time. Just before noon
the drill he was operating stopped rotating because the drill
bit had become wedged in the hole. Moore and Ronald
Cunningham, driller's helper, attempted to free the bit by
rotating and pulling the string of approximately 40 rods with
the drill. Unsuccessful at this, and with the assistance of
job superintendent Daniel Mayberry, they attempted to free
the bit by using the pipe wrenches. Cunningham and Mayberry
used one wrench with a six-foot cheater pipe to twist the
rods while Moore braced the handle of the other wrench
against the drill frame to maintain the incremental torque
gained.
At about 12:15 p.m., after twisting the string of rods one-half to one revolution without freeing the bit, the three men
decided to discontinue the effort. When the cheater pipe was
removed, the back-up wrench slipped and built-up torque was
released. The other wrench rotated around the rod striking
Moore on the arm and head.
Emergency Medical Technicians were immediately summoned to
assist Moore. He was transported by ambulance to a hospital
in Elko, Nevada and then transferred to a medicial facility
in Salt Lake City, Utah. He died on April 14, 1996 in a
convalescent home near his residence in Upton, Wyoming.
CONCLUSION
The cause of the accident was the improper use of the pipe
wrench. By placing the cheater pipe extension on the handle,
the wrench was used beyond its design capacity.
VIOLATIONS
Citation No. 4141245, 104(a), Part 57.14205
Issued March 18, 1996.
Three drilling employees were attempting to free a 400 foot
string of drill rods that was stuck in the drill hole. This
was done by using two 24-inch pipe wrenches,one with a 6-foot
long cheater pipe. The drill rods were torqued about 1/2 to
1 revolution when one of the wrenches slipped. The other
wrench rotated, striking one of the employees and causing
serious head injuries. These pipe wrenches are not designed
to hold the amount of torque applied.
This citation was terminated on March 18, 1996. Company
policy now prohibits the use of pipe wrenches for freeing
drill rods. A string of smaller dimension rods, with a
Diamond Drill Cutter at the end, will be inserted in the
stuck rods and extended to the point where the bit is to be
cut off. Rotating this cutting device will result in the bit
being removed at its base.
/s/ Michael J. Drussel
Mine Safety and Health Inspector
Approved by:
Fred M. Hansen, Manager,
Western District
Related Fatal Alert Bulletin: [FAB96M11]
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