UNITED STATES
DEPARTMENT OF LABOR
MINE SAFETY AND HEALTH ADMINISTRATION
Accident Investigation Report
Surface Nonmetal Mine
Fatal Machinery Accident
Yakima - Pre-Mix #6
Central Pre-Mix Concrete Company
Yakima, Yakima County, Washington
Mine ID No. 45-00995
January 8, 1997
by
Dennis D. Harsh
Mine Safety and Health Inspector
Arnold E. Pederson
Mine Safety and Health Inspector
Mine Safety and Health Administration
Western District
3333 Vaca Valley Parkway, Suite 600
Vacaville, California 95688
Fred M. Hansen
District Manager
GENERAL INFORMATION
David Allen Kroll, mechanic/repairman, age 37, was fatally
injured about 12:30 p.m. on January 8, 1997 when the blade
mill in which he was working started up. Kroll had a total
of one year and five months of mining experience, all with
this company. He had not received training in accordance
with 30 CFR Part 48.
Wayne Kalbfleisch, vice president of Central Pre-Mix
Concrete, notified MSHA at 1:40 p.m. on the day of the
accident. An investigation was started the following day.
Yakima Pre-Mix #6, a Sand and Gravel wash plant owned and
operated by Central Pre-Mix Concrete Company, was located at
Yakima, Yakima County, Washington. Principal operating
officials were Wayne Kabfleisch, vice president, Mike
Besancon, superintendent, and James Blevins, plant foreman.
The wash plant normally operated one 10-hour shift, five
days a week. A total of three persons worked at the plant.
Sand and gravel was transported by over-the-road trucks from
an off-site pit to the plant for washing and screening. The
material was then transported by conveyors to stockpiles.
The finished product was sold, or used to supply the
company's ready mix operation located adjacent to the wash
plant.
The last regular inspection of this operation was completed
on July 23, 1996.
PHYSICAL FACTORS
The accident occurred inside a Model 6500 blade mill built
by Kolberg Products. The mill, used to pre-condition
aggregates prior to wet screening, was 22 feet 5 inches
long, 7 feet wide, and 10 feet high. It was supported,
about 18 feet above ground, by a substructure of I-beams.
The mill was inclined about 15 degrees and had a railed work
deck on three sides. The deck, about two feet above the
base of the mill, was accessed by a vertical ladder. The
top of the mill was about 8 feet above the work deck and
could be reached with a portable ladder.
Blades and flights on the mill were 36 inches in diameter
and attached to twin screws. The blades were replaceable
NI-HARD paddle tips bolted onto NI-HARD outer wearing shoes.
The shoes were on spiral flights that provided a scrubbing
and abrading action to break up and dissolve waste material.
The mill's twin screws were belt driven by two 40 hp.,
electric motors operated from a control center in a trailer
about 100 feet from the mill.
The wash plant, including the mill, was controlled by
General Electric Fanuc series 90-30/90-20 micro processors,
Programmable Logic Controller(PLC), that received power from
a 230/120 volt panel board. The panel board's main
disconnect was a 230 volt, two pole, 125 amperes circuit
breaker. For the past week an internal heat problem had
caused the breaker to trip after about 10 to 15 minutes of
operation. This would result in a loss of control power to
wash plant components.
The wash plant control panel contained two emergency stop
switches, a start-up warning switch, and start/stop stations
for the individual motors within the plant.
A modification to the PLC in October of 1996 resulted in
power being unintentionally returned to components following
a power failure, if their switches had been left in the "on"
position.
DESCRIPTION OF ACCIDENT
David Allen Kroll (victim) started work at 7:30 a.m. on
January 8, 1997, his regular starting time. He was assigned
to work with James Blevins, wash plant foreman. They were
to thaw the frozen material inside the blade mill and then
replace broken and worn paddle tips and wearing shoes.
Kroll removed the plywood sheets that had been placed on top
of the mill to retain heat generated by a propane heater
located below. He signaled Blevins, who was at the motor
control, to start the two blade mill motors, one at a time,
to see if they were free of frozen material. Blevins
started the mill motors, as well as those for the stacker
conveyor and the feeder belt. Satisfied that the mill was
free of ice and frozen material, Blevins loaded some empty
propane tanks onto a truck to take them to a fill station
located across the property.
Before leaving with the tanks Blevins returned to the motor
control center and switched the four start/stop button
switches to the "off" position, stopping all four motors
that he had started earlier. Blevins left at approximately
8:15 a.m., while Kroll was preparing to make repairs in the
mill, and returned about 9:00 a.m. He and Kroll worked
together about two and one-half hours.
About 11:45 a.m. a contract electrician, Paul Riel, arrived
and Blevins went with him to check out a faulty breaker.
Kroll remained in the mill. Blevins and Riel went to a 125
amp breaker that, for the past week, had been tripping out
after being engaged 10 to 15 minutes. This breaker
controlled numerous smaller breakers such as those for
control center lighting, receptacles, and PLC power.
Blevins reset the tripped breaker and Riel observed its
operation for a few minutes. He then told Blevins he would
remove the metal panels and tighten the terminal lugs and
take ammeter readings to see if he could determine what was
wrong. Reil turned the breaker off, removed the panels and
proceeded to troubleshoot the panel board. He determined
that the circuit breaker had an internal heat problem and
would replace it the following morning.
Ten to fifteen minutes after Riel started troubleshooting,
Blevins left to check on Kroll. As he was leaving the motor
control center he glanced over at the control panel and
noticed that the two blade mill buttons were in the "run"
position. He pushed them down to the "off" position then
continued to the blade mill. He found Kroll inside the
mill, entangled in the blades. Blevins informed Riel of the
accident and then drove to the shop to call 911. Within 2
to 3 minutes paramedics arrived. Kroll was pronounced dead
at the scene.
Information gathered during the investigation suggests that
Kroll turned on the blade mill to clear some remaining
frozen material after Blevins left to refill the propane
tanks. The mill operated until the 125 Amp breaker heated
up and kicked out. Kroll then went back to work in the mill
without shutting off any switches. Because the PLC was
incorrectly programmed, the mill began operating when the
125 amp breaker was reset during troubleshooting of the
electrical system.
CONCLUSION
The primary cause of the accident was the failure to lockout
the two-blade mill electrical disconnects prior to working
on the mill.
A contributing factor was the mis-programming of the
Programmable Logic Controller which permitted equipment to
be inadvertently energized without warning.
CITATIONS/ORDERS
Order No. 4364005
Issued on January 9, 1997 under
provisions of Section 103(k) of the Mine Act:
On January 8, 1997 a blade mill became energized and fatally
injured a mechanic working inside the mill. This order was
issued to insure the safety of persons until the affected
areas of the mine could be returned to normal operation
This order was terminated on January 10, 1997 after the PLC
was properly programmed.
Citation No. 7950070
Issued on January 9, 1997 under
provisions of Section 104(d)(1) for violation of 30 CFR
56.12016:
On January 8, 1997 a mechanic was fatally injured while
working inside a Kolberg blade mill when it inadvertently
started. The two 480 volt, 3 phase, blade mill drive motors
were energized through Allen Bradley starters that were
located in a motor control center trailer. Power to the two
100 amp circuit breakers for the motors was not locked out
nor were other measures taken to prevent the equipment from
becoming energized without the knowledge of the individuals
working on it. The plant foreman was aware that the motor's
circuits were not locked out and he was involved with mill
repairs. This is an unwarrantable failure.
This citation was terminated on January 9, 1997 after the
company re-emphasized with their employees their requirement
for equipment lock-out.
Citation No. 7950071
Issued to H&N Electric Inc.,
contractor ID 2GS, under provisions of Section 104(a) of the
Mine Act for violation of 30 CFR 56.12002:
On January 8, 1997 a mechanic was fatally injured while
working inside a Kolberg blade mill that was not locked out
and was inadvertently started. A General Electric Funac
series 90-30/90-20 micro (PLC) programmable logic controller
was used to control power to plant electrical equipment.
Last October (1996) a normally open contact button was
incorrectly installed in the program. This contact
prevented run mode restarting of the timing control and
would allow unintentional start up when power was restored
after an outage.
This citation was terminated on January 10, 1997 after
corrections were made to the segment of the electrical
system that was permitting unintentional start-up.
/s/ Dennis D. Harsh
mine safety and health inspector
/s/ Arnold E. Pederson
mine safety and health inspector
Approved by: Fred. M. Hansen, District Manager
Related Fatal Alert Bulletin: [FAB97M01]
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