UNITED STATES
DEPARTMENT OF LABOR
MINE SAFETY AND HEALTH ADMINISTRATION
Northeast District
Surface Nonmetal Mine
(Crushed Stone)
Fatal Explosive Accident
Dyno New England, Inc.
ID No. B6Z
at
The York Hill Traprock Quarry Company, Inc.
The York Hill Mine and Mill
I.D. No. 06-00026
Meriden, New Haven County, Connecticut
July 16, 1997
By
Michael J. Music
Supervisory Mine Safety and Health Inspector
and
Edward M. Blow
Mine Safety and Health Inspector
Northeastern District Office
230 Executive Drive, Suite 2
Cranberry Township, Pennsylvania 16066-6415
James R. Petrie
District Manager
GENERAL INFORMATION
Joel Kanute, lead blaster, age 43, was fatally injured at approximately 7:45 a.m., on July 16, 1997,
and Arthur "Skip" Sibley, Jr., age 38, general manager, was seriously injured, when a premature
detonation occurred while they were trying to dislodge a cartridge of dynamite that had hung up
in a blast hole. Both individuals were employed by Dyno New England, Inc., an independent
contractor specializing in blasting. Kanute had 4« years with this company, and 17 years
experience in handling explosives. Sibley also had 4« years with this company, and 18 years
experience in handling explosives. Kanute and Sibley had received training in accordance with
30 CFR Part 48.
Cheryl Suzio, safety coordinator for The York Hill Traprock Quarry Company, Inc., notified
MSHA at approximately 8:40 a.m. on the day of the accident. An investigation was started the
same day. The last regular inspection of The York Hill Traprock Quarry Company, Inc., was
completed on May 16, 1997. Another regular inspection was conducted after the conclusion of
this investigation.
The York Hill Mine and Mill was a multiple bench, crushed stone, operation with an associated
mill, owned and operated by The York Hill Traprock Quarry Company, Inc., and located in
Meriden, New Haven County, Connecticut. The principal operating official was Leonardo C.
Suzio, president. The facility normally operated one, 9-hour shift per day, 5 days per week, and
employed a total of 10 persons.
Dyno New England, Inc. was contracted to do the blasting at The York Hill Mine and Mill. The
principal operating official was H. Dean Mitchell, president. Dyno New England, Inc. was
located in Middlefield, Connecticut, and employed a total of 50 persons, four of whom were
working at the mine on the day of the accident. Dyno New England, Inc. worked at this property
approximately 1 day per week, every other week.
At the mine, traprock was drilled, blasted, and then loaded into off-road haul trucks utilizing
front-end loaders. The trucks transported the material from the pit to the mill where it was
crushed and sized. The finished products were loaded onto over-the-road trucks for transport to
customers.
PHYSICAL FACTORS
The quarry where the accident occurred consisted of seven benches with an inclined haul road at
the north-northeast end. The explosion occurred on the sixth bench and Kanute fell over the
46-foot highwall to the fifth bench.
The blast pattern consisted of 21 holes laid out in a triangular shaped blast pattern. Most of the
holes were drilled on an 11-foot by 11-foot spacing and burden, however, the spacing between
several of the holes near the highwall edge was less than 11 feet due to irregularities in the
highwall face. These front holes were angled between 4 and 5 degrees to achieve an 11-foot
burden at the bottom of the hole. Each blast hole was 4 inches in diameter and 51 feet deep. The
holes were laid out and drilled by the drilling contractor, Dearco Drilling, Inc. The ground where
the blast pattern was laid out was basically level with visible cracks near the edge of the highwall.
The blast hole which prematurely detonated was located near the southeast corner of the blast
pattern and was approximately 7 feet from the edge of the highwall. It was drilled straight and
was not one of the angled holes.
The loading and initiation of the 21 holes was planned for the morning of July 16, 1997, by Dyno
New England's blast crew. Each member of the crew had handled explosives in this quarry on
several previous occasions.
The explosive which had hung up in the hole was a 3«-inch diameter by 16-inch long cartridge of
Gelaprime F brand gelatine dynamite, 85% strength, containing nitroglycerine, and weighing
8 pounds. It was manufactured by Dyno Nobel, Inc., in Joplin, Missouri, and the lot had a
date/plant/shift code of 04JU97J1-44599. This product was not manufactured with a bail for
lowering into boreholes.
The Nonel (non-electric) brand detonators, used to assemble the primers, were manufactured by
Dyno Nobel, Inc. in Port Ewing, New York, and came attached to a 60-foot length of shock tube.
A primer was assembled by punching two holes in a cartridge of Gelaprime F , one through the
cross section of the cartridge, and the other in the priming end of the cartridge. The detonator
was then passed through the cross-hole and into the priming end.
The company's procedure for loading the blast holes in this quarry was as follows:
(1) Four cartridges of 3«-inch by 16-inch Gelaprime F were dropped to the bottom of
the hole;
(2) A primer, assembled as described above, was then lowered into place;
(3) A cartridge of 3«-inch by 16-inch Gelaprime F , weighing approximately 8 pounds,
was then dropped on top of the primer;
(4) The hole was bulk loaded with an emulsion blasting agent up to approximately 12 to
15 feet from the top of the hole;
(5) A second primer, consisting of a 2-inch by 16-inch cartridge of Gelaprime F and a
Nonel detonator, was lowered on top of the blasting agent; and,
(6) The explosive material column was brought up to 10 feet from the hole collar using
Blastex , a cartridge emulsion.
Members of the blast crew, however, were not consistently following the above loading
procedure, and would vary the placement of the primer among the five cartridges at the bottom of
the hole.
It is not known how many cartridges of explosives Kanute had loaded into the hole prior to the
one which hung up. Sibley, who had come over to assist Kanute free the hang-up, stated that the
cartridge which hung up was the only one in the hole, and that the hole did not contain a primer.
A blast crew member who had witnessed the accident stated to police that Kanute and Sibley had
already lowered five cartridges of explosives into the hole, and were lowering the primer when it
hung up. Evidence observed and collected at the accident scene, however, did not confirm either
account regarding the location of the primer.
The evidence supports a finding that, at the time of the accident, a primer was located near the
bottom of the hole, and that the shock tube from the primer's detonator was strung the length of
the hole with several feet exposed on the surface. Additionally, it supports a conclusion that a
cartridge of dynamite had hung up near the top of the hole and that impacting it with the loading
pole caused it to detonate. When the cartridge detonated, the explosive shock traveled the length
of the shock tube to the bottom of the hole, setting off the primer and other cartridges of
explosives. The detonation of the cartridge near the top of the hole also produced a small crater
on the surface surrounding the hole.
A piece of shock tube, 4-feet 3-inches long, which had been fired, was found near the blast hole.
It was determined that the remaining 55-feet 7-inches of the shock tube was in the blast hole at
the time of the accident and had disintegrated in the explosion. If the primer had been located
near the top of the hole as one witness stated, rather than near the bottom, most of the shock tube
should have been found intact on the surface.
Following the accident, the other holes in the blast pattern were loaded and the entire shot was set
off. After clearing the muck from the blast site, the remnant of the hole involved in the premature
detonation was found in the floor of the quarry. Examination of this hole revealed the presence of
explosive residue, and fracturing and expansion of the ground surrounding the hole. This
supports the finding that explosive charges had been located in the bottom of the hole and that
they had detonated. Alternatively, if the bottom of the hole did not contain any explosives as
claimed by Sibley, there should have been little or no explosive residue found, and the ground
immediately surrounding the hole would not have exhibited direct blast damage.
Prior to the accident, Kanute and Sibley had used a retrieving tool to try and extract the hung up
cartridge from the hole. This tool was 7 inches long and had 6 pointed brass barbs at the end
whose function was to grab the product to be retrieved. It contained a ball which fit into the
socket end of the loading pole. Sibley stated that the retrieving tool had come off the pole and
was lost down the hole, however, he could not recall if it had broken off or become detached
from the socket. The use of this retrieving tool and subsequent impacting with the loading pole,
presumably introduced grit into the explosive material. Information provided by a manufacturer
of nitroglycerin-based explosives, and Bureau of Mines' Circular No. 54, indicates that the
introduction of grit into nitroglycerin-based explosives can make them more sensitive to impact.
The loading pole, which was being used by the victims at the time of the accident, was wooden,
1¬-inch in diameter, with aluminum ball and socket connectors. Reportedly, the pole was
16 feet in length when purchased. Two sections were recovered, one 5-feet, 4«-inches long and
the other 3-feet, 1-inch long. The condition of the tip of the loading pole just prior to the
explosion was not known. If the retrieving tool had broken off, the tip of the pole may have been
bare wood. If it had become detached from the socket, the tip of the pole would have consisted
of an aluminum socket. Sibley stated that his arms had become fatigued by his effort to free the
cartridge using the loading pole. Additionally, a blast crew member who had witnessed the
accident stated to police that Kanute and Sibley were impacting on the explosives heavily with the
loading pole when it detonated.
Neither Kanute or Sibley were wearing a safety belt and line at the time of the accident, and none
were worn by any of the four-man crew that morning while loading holes that were within
3 to 4 feet of the edge of the highwall. The contractor had been cited several times previously,
and once at this same quarry, for failure to use safety belts and lines. The company president had
sent a letter to all employees approximately a month before the accident, stating that they were
expected to use a safety belt and line when working near the edge of a highwall. However, this
blast crew, which included the two agents of the contractor who were involved in the accident,
chose to ignore these instructions.
When the blast crew arrived at the quarry, they found a very thick, low fog condition, making it
difficult to find their way to the blast site. There was no electrical activity in the immediate area at
the time of the accident.
DESCRIPTION OF ACCIDENT
On the day of the accident, the blasting crew consisting of Joel Kanute, lead blaster, (victim),
Arthur "Skip" Sibley, Jr., general manager, (injured), William Ripley IVth, powder truck driver,
and Jonathan Handley, bulk truck driver, arrived around 6:00 a.m. Kanute assigned the crew to
check, measure, and load holes beginning about 6:25 a.m. Loading progressed normally until
approximately 7:30 a.m., when Kanute had a cartridge of explosives material hang up in one of
the holes he was loading.
Sibley finished the hole he was loading then went over to assist Kanute. After they unsuccessfully
tried using a loading pole to dislodge the stuck cartridge, they attached a retriever tool and tried
to extract the explosive material. However, the tool either broke off or became detached from the
pole and remained in the hole. They then resumed impacting the explosives using the loading
pole. The use of the retrieving tool, and continued use of the loading pole after the retrieving tool
had been lost down the hole, presumably resulted in the cartridge being punctured and
contaminated with dirt and grit from the hole.
At about 7:45 a.m., while they were using the loading pole to try and dislodge the cartridge, a
detonation occurred. Kanute took the main force of the blast and fell over the 46-foot highwall.
Handley, who was loading the hole directly behind the one which detonated, caught Sibley who
had stumbled backwards, while noticing Kanute falling over the face. Handley, a trained EMT,
administered first-aid to Sibley, who was seriously injured in the blast. He then proceeded to his
truck and called 911, while Ripley stayed with Sibley. After Handley returned, Ripley went down
to the 5th level and administered first-aid to Kanute until two ambulances arrived a short time
later.
Kanute was transported via ambulance to a local hospital where he was pronounced dead. Sibley
was stabilized and transported via a second ambulance to the local hospital where he spent several
weeks recovering.
CONCLUSION
The primary cause of the accident was the impacting on the dynamite with a loading pole. The
failure to wear a safety belt and line while working where there was a danger of falling
contributed to the severity of the accident.
RECOMMENDATIONS
A formal written procedure for handling hung explosives should be developed and followed.
Once a cartridge of explosives becomes firmly lodged in a hole, efforts to dislodge it should be
discontinued, and the hole top primed and fired with the rest of the round.
Additionally, loading procedures for each shot should be established and consistently followed by
all members of the blast crew.
VIOLATIONS
Order No. 4569386
Issued on July 16, 1997, at 8:40 a.m., under the provisions of Section
103(k) of the Mine Act:
A premature detonation of explosive charges has occurred on the No. 6 bench of the
quarry resulting in the death of a contract blaster and the serious injury of another contract
miner who were attempting to prepare a multi-round charge to be fired. This order
prohibits the use of explosives and blasting agents or any work on or near the No. 6 bench
area pending an investigation by MSHA to determine if any additional hazards remain in
the area for the safety of all parties involved in this investigation.
The order was modified on July 17, 1997, at 2:00 p.m., to allow the contractor to finish charging
the remaining holes and detonate the shot. The order was terminated on July 18, 1997, 6:30 a.m.,
following the safe firing of the shot.
Citation No. 7704722
Issued to Dyno New England Inc. on September 30, 1997, under the
provision of Section 104 (d) of the Mine Act, for violations of 30 CFR 56.6905(b):
A fatal accident occurred at this operation on July 16, 1997, when a premature detonation
occurred while two contract blasters were trying to dislodge a cartridge of dynamite that
had hung up in a blast hole. The lead blaster was killed and the general manager was
seriously injured. Prior to the blast, they had unsuccessfully tried to use an extractor to
retrieve the cartridge, but they had lost the tip in the hole. They then resorted to using a
loading pole to try and dislodge the cartridge, and were impacting on it with the pole
when the detonation occurred. This procedure may have resulted in grit being introduced
into the explosive material, increasing its sensitivity to impact. The hazards of impacting
on explosives is widely known among blasting contractors and the actions of these agents
represented a serious lack of reasonable care constituting aggravated conduct and
unwarrantable failure.
This citation was terminated on September 30, 1997, after the company put forth a policy on
impacting on explosives and has instructed all of their employees on it.
Citation No. 7704723
Issued to Dyno New England Inc. on September 30, 1997, under the
provision of Section 104(d) of the Mine Act, for violations of 30 CFR 56.15005:
A fatal accident occurred at this operation on July 16, 1997, when a blast hole prematurely
detonated while two contract blasters (lead blaster and general manager) were trying to
dislodge a cartridge of dynamite that had hung up in the hole. The general manager was
severely injured in the explosion, and the lead blaster died from the force of the explosion
and fall from the highwall. The blast hole was located approximately 7-feet from the edge
of the 46-foot highwall, and cracks were visible near the edge. Neither victim was
wearing a safety belt and line at the time of the accident, nor anytime that morning while
loading holes that were even closer to the edge. The contractor had been cited several
times previously, including once at this same quarry, for not using safety belts and lines.
The failure of the lead blaster to wear a safety belt and line contributed to the severity of
his injuries. The action of these agents constituted a reckless disregard of the standard and
unwarrantable failure to comply.
This citation was terminated on September 30, 1997, after the company provided all of their
employees with safety harnesses and lines, and instructed them to use them where there is a
danger of falling.
//s/ Michael J. Music
Supervisory Mine Safety and Health Inspector
//s/ Edward M. Blow
Mine Safety and Health Inspector
Approved by: James R. Petrie, District Manager
Related Fatal Alert Bulletin: [FAB97M38]
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