Capital Coal Corporation's Mine No. 5 is located .95 miles west of Pilgrims Knob approximately 300 feet south of Route 638 on Dismal Creek in Buchanan County, Virginia. Production began on November 11, 1997, with four drift openings into the Jawbone Coal Seam, which locally averages 3.5 feet in thickness. The immediate mine roof consists of approximately 6 inches of shale which is overlain by a main roof of sandy shale and sandstone. The mine is eight entries wide and 1600 feet deep. Ventilation is provided by a single exhausting fan installed in the No. 4 Drift which produces approximately 83,000 cubic feet per minute of air. The latest laboratory analysis of return air samples at the fan showed a total methane liberation of 79,810 cubic feet per day. The face areas are ventilated using a double split system of ventilation and exhausting line curtains.
Employment is provided for 11 underground and 2 surface personnel. The mine operates one shift per day, five days a week to produce 450 tons of coal per day from a single Mechanized Mining Unit (001-0). A room and pillar system of mining is employed using continuous mining machines, shuttle cars, scoops, and single and dual head roof bolting machines. Coal is transported from the faces by shuttle cars, and out of the mine via belt conveyor. A battery-powered track haulage system is used to transport both personnel and materials.
The Roof Control Plan in effect at the time of the accident was approved by the Mine Safety and Health Administration (MSHA) on October 9, 1997. The Roof Control Plan requires, as a minimum, the installation of four foot resin grouted roof bolts on a four foot by four foot pattern. Maximum entry and crosscut widths are 20 feet in all entries and crosscuts, except the belt and track entry which is limited to 22 feet in width. Entry and crosscut centers from 60 to 100 feet are permitted with extended centers of up to 200 feet permitted in adverse conditions. Roof test holes are required to be drilled at intervals of 20 feet and are to be drilled at least one foot deeper than the length of the bolt being used.
The Training Plan was approved by the MSHA District Manager on September 5, 1997. The Plan includes provisions requiring training on the Roof Control Plan.
The principal officials for Capital Coal Corporation at the time of the accident were:
| President: | Hank K. Matney | |
| Vice President: | Rick A. Matney | |
| Secretary/Treasurer: | Fred Matney | Mine Superintendent: | Ray Kinder |
An MSHA Safety and Health Inspection (AAA) was completed on August 5, 1998 and another was ongoing at the time of the accident.
The third quarter fiscal year 1998 incidence rate for the mining industry was 8.89 as compared to 0.00 for this mine.
On Thursday, December 3, 1998, the coal production crew under the supervision of Eddie Looney, section foreman, entered the mine at 7:05 AM. The crew proceeded with normal production activities which included the operation of two dual head roof bolting machines by a two person crew and a single head machine operated by one person. These activities included cutting and roof bolting approximately eight places, three of which were bolted by Danny Lester (victim) using the single head Model LRB-15A Long Airdox Roof Bolting Machine. Plans for that day included some of the crew staying after the end of the shift to cut a trench with the continuous mining machine along the No. 7 Entry to direct water to a sump between Nos. 7 and 8 Entries.
At approximately 12:00 Noon, Ray Kinder, superintendent, came underground via a battery powered scoop. He delivered supplies to all three roof bolting machines and unloaded the remaining supplies in the supply hole. The last known contact with the victim was by Kinder at approximately 2:00 PM when he supplied Lester's roof bolting machine just before Lester entered the No. 3 Entry to begin roof bolting the place. Kinder then assisted moving the continuous mining machine to the No. 5 Entry. At approximately 2:30 PM, Looney and Kinder began making preparations to cut the trench. Looney began replacing bits on the continuous mining machine while Kinder began hanging line curtain in the No. 7 Entry to ventilate the trenching operation.
At approximately 3:00 PM, as the remainder of the crew was preparing for the end of the shift, Eddie Brown, one of the roof bolting machine operators for the dual head machines, went to the other dual head machine to retrieve his coat. As he passed the opening to the No. 3 Entry, he heard the single head machine still running in the face area of the entry. He signaled with his cap light and called to Lester, the machine operator, but received no response. Brown went to the roof bolting machine where he found Lester at the front of the machine at the drill controls. Lester was in a kneeling position with his head caught between the ATRS and the frame of the machine which protruded forward of the panic bar. Brown saw a cardboard box containing resin grout tubes on top of the ATRS levers. He removed the box and activated the tilt jack lever, resetting the ATRS to an approximately vertical position. Brown raised Lester up and upon seeing the extent of Lester's injuries, he immediately left the place and traveled toward the mantrip yelling for help.
Looney was in the No. 7 Entry setting bits on the continuous mining machine when he heard Brown yelling that Lester was seriously hurt. Looney went to Brown who informed him of Lester's location. Looney, a First Responder, immediately went to the No. 3 Entry Face where he found Lester at the drill controls. He called Lester's name several times and, receiving no response, he checked Lester's neck for a pulse but could detect none. Not knowing that Brown had raised the ATRS, Looney did not know how Lester had been injured. He raised Lester's head and saw that he had severe head injuries. He yelled to Kinder that Lester was injured and for Kinder to come to him.
Kinder had been in the No. 7 Entry when he first overheard Brown saying that someone was injured. As he traveled toward Brown, he heard Looney yell to him and he proceeded directly to the accident scene. Looney directed the crew to have someone outside call for an ambulance and for the crew to bring the first aid box. Kinder asked about Lester's condition and was informed that he was seriously injured. The two men then moved the victim away from the machine and placed him on the mine floor. Looney tilted the victim's head back and examined him for signs of breathing. He again checked the victim for a pulse and found none. Looney stated that a more complete visual examination revealed massive head injuries. The victim was strapped to a backboard and transported by scoop to the end of the track. He was then transferred to a rail vehicle and subsequently transported to the surface of the mine. The Dismal River Rescue Squad transported the victim to Buchanan General Hospital where, at 4:38 PM, he was pronounced dead on arrival by the county medical examiner, Dr. Segen.
The roof bolting machine had a two section hydraulic pump. The 9 Gallon Per Minute (GPM) section supplied flow for the control valve which controls the ATRS functions and the drill and cable reel control valve which controls the stabilizer, the drill boom lift, and the cable reel. The flow from this pump section went to the ATRS control valve before going to the drill and cable reel control valve located at the drill station. The 28 GPM section supplied hydraulic flow for the tram and drill rotate circuit. The flow from this pump section went to the tram valve before it went to the drill rotate valve located at the drill station
The ATRS lift jacks were held in place against the roof by the load locking valves attached to the bottom of the ATRS lift jacks. Once the control valve, which activated the ATRS lift jacks, was released, there was no further flow to keep the ATRS tight against the roof.
Tests were conducted which determined the ATRS tilt jack could not fold the ATRS back onto the drill boom, if the ATRS was tight between the mine floor and roof. Although the ATRS could not be folded back when it was tight against the roof, the ATRS loosened from the roof and could be folded back when, during bolting operations, a hole was drilled in the roof. One reason this happened was the flow from the 9 GPM pump section went to the ATRS control valve, before going to the drill and cable reel control valve. This caused hydraulic pressure to build inside of the ATRS control valve when the drill boom lift section was activated. When a hole was drilled, the pressure generated inside of the ATRS control valve would cause hydraulic flow to bypass the spool in the lift section of the ATRS control valve. The hydraulic flow that bypassed the spool would enter the lift jack of the ATRS and apply pressure to the pilot operated release mechanism of the load locking valve. This action released the load locking valves, which allowed the ATRS to loosen from the roof. Another reason for the ATRS to loosen from the roof was a leaking load locking valve on the left lift jack. This problem, which would contribute to loosening of the left side of the ATRS, was found during tests of the ATRS lift jacks at a hydraulic machine shop.
The accident occurred because the unprotected ATRS tilt jack control lever was unintentionally actuated by a falling box of resin grout tubes. The ATRS support surfaces were not set firmly against the mine roof, allowing the tilt jack to rapidly fold the ATRS inward toward the front of the machine, crushing the victim against the machine.
The following orders/citations were issued due to conditions revealed during the investigation.
Respectfully submitted:
Roy D. Davidson
Electrical Engineer
Arnold D. Carico
Mining Engineer
Approved:
Ray McKinney
District Engineer
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