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U.S. Department of Labor Mine Safety and Health Administration Protecting Miners' Safety and Health Since 1978 |
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UNITED STATES
DEPARTMENT
OF LABOR
MINE
SAFETY AND HEALTH ADMINISTRATION
COAL
MINE SAFETY AND HEALTH REPORT OF INVESTIGATION Underground Coal Mine Fatal Machinery Accident at Air Quality #1 Mine Black Beauty Coal Company Wheatland, Accident Investigators Michael D. Rennie Coal Mine Safety and Health Inspector Arthur D. Wooten Coal Mine Safety and Health Inspector (Electrical) Leland Payne Educational Field Services Robert J. Holubeck Brian Malin Originating Office - Mine Safety and Health
Administration District 8 James K. Oakes, District Manager On The cause of the accident was the failure to ensure that
all workers followed the safety precautions contained in the mine’s approved
Roof Control Plan in regard to not standing or walking between the continuous
mining machine and the coal rib while the machine is in motion. The victim was
located in a pinch point created by the continuous mining machine and the coal
rib.
Black Beauty Coal Company’s Air Quality # 1 Mine is located 2.3 miles
southwest of Wheatland, The mine produces an average of 16,000 tons of raw coal per
day from four advancing continuous mining sections. Coal is extracted
from the faces by Joy 14CM remote controlled continuous mining machines.
Electric shuttle cars and/or battery ramcars transport the coal to the section
loading point, where the coal is then transported from the section to the
surface by a series of belt conveyors. The face areas are ventilated by blowing
line curtains and scrubber-equipped continuous mining machines. The mine is ventilated by two mine fans and liberates
627,217 cubic feet of methane per day. The immediate mine roof consists of 10 to 30
feet of gray shale, and the overburden is a maximum of 350 feet. Roof support is
installed using roof bolting machines equipped with automated temporary roof
support systems. The Training Plan that was in effect at the time of the
accident was approved on The principal officers for the Air Quality #1 Mine at the time of the accident
were: President...........................................................................
Daniel Hermann
Superintendent ..................................................................
Douglas Grounds
Engineering Manager.......................................................
Jonathon Dever
Safety Director..................................................................
Ronald Madlem An MSHA Safety and Health Inspection, AAA, began on
The
calendar year 2003 National Non-Fatal Days Lost (NFDL) incidence rate for
underground coal mines was 5.93 and the NFDL incidence rate for this mine was
6.62.
On The third shift maintenance crew for the No. 4 Working
Section arrived on the section at approximately Robinson first examined the areas where work was to be
performed, and then the maintenance crew began moving the mining equipment from
the left-side rooms to the entry faces. The right-side continuous mining machine
was moved to the No. 7 Entry and the left-side continuous mining machine was
moved to the No. 3 Entry. The roof bolting machine was moved to the No.
6 Entry. Keith Scott and Christopher Qualls, Mechanic/Electricians,
started servicing the right-side continuous mining machine. Robinson, Tim
Williams, and Ben Smith, both laborers, were working at the belt tail moving and
repositioning the ratio feeder. When the servicing work was almost complete on
the right-side continuous mining machine, Qualls informed Scott that he was
going to go to the roof bolting machine to check the hydraulic oil level and
then travel to the left-side continuous mining machine to prepare it for
servicing. After Scott had completed the work on the right-side
continuous mining machine, he traveled directly to the left-side continuous
mining machine where he found Qualls crushed between the discharge boom of the
continuous mining machine and the right coal rib. Scott stated that no more than
five minutes had elapsed between when Qualls had left the right-side continuous
mining machine until he found him crushed against the rib. After finding Qualls crushed against the rib, Scott ran to
the belt entry and yelled for Kris Robinson. Scott informed Robinson that Qualls
was seriously hurt. He then proceeded to the mine phone and
contacted the surface for assistance. Robinson instructed Williams to get the
first aid equipment and then to meet him at the left-side continuous mining
machine. Ben Smith went to the phone and notified the surface of the
accident. Robinson ran to the left-side continuous mining machine
where he found Qualls crushed by the discharge boom against the coal rib. Robinson, Scott,
and Williams maneuvered beneath the boom and removed the remote control unit
from Qualls. Robinson and Williams held Qualls while Scott
used the remote control unit to swing the boom away from Qualls. After freeing him
from the boom, Robinson immediately checked Qualls but found no signs of life.
Cardio pulmonary resuscitation (CPR) was started by Robinson and Williams. Jesse Emmons, Advanced EMT, was dispatched to the working
section and upon arrival took over care of the victim. CPR continued while
Qualls was being transported out of the working section to the Hart Street
Portal bottom, where Halter/Smith Ambulance Service paramedics assumed care of
the victim. Qualls was then transported to Good Samaritan Hospital in
Ron Madlem, Safety Director, reported the accident to
the Mine Safety and Health Administration (MSHA) Vincennes Field Office
Supervisor, Gary W. Jones, at approximately A joint investigation was conducted by MSHA and the
Indiana Bureau of Mines to determine the cause(s) of the accident and to
prevent a similar occurrence. Before traveling to the accident scene,
the investigation team held preliminary interviews with persons who were
on the working section at the time of the accident. The team examined the
immediate area where the accident occurred. The accident area and
equipment were photographed and measurements were taken at the scene. Training
records, examination records, and work practices relative to the accident
were reviewed. The continuous mining machine involved in the accident was
put through operational tests to verify if it was functioning properly at
the time of the accident. No functional defects were observed
during these tests. Investigators tested and evaluated various parts of
the equipment that were involved in the accident. A list of the sites,
equipment, and dates of these evaluations and tests are listed below: Accident Site, May 19 and 20, 2004 Magnetek – Power Control Systems, Approval and Matric Limited, Joy Mining Machinery, Black Beauty Coal Co. Air Quality #1 Mine,
1.
There were no eyewitnesses to the accident. 2.
The victim was moving the left-side continuous mining
machine located in the No. 3 Entry back from the working face. At the
accident location, the victim may have been trying to reposition or change
direction of the machine when the accident occurred. (See Appendix C) 3.
The front of the continuous mining machine was
located 87 feet from the No. 3 Entry face. 4.
The mine floor in the immediate area was dry and
smooth with a very small change in elevation. 5.
The seam height in the immediate area was 6 ½
feet. 6.
The entry width at the rear bumper of the continuous
mining machine was 19-feet 2-inches (See Appendix D) . The diagonal measurement of the No. 29
Crosscut intersection averaged 31-feet. 7.
The Joy continuous mining machine, Model No.
14CM-15-11DX, Serial No. JM 4631C, Company No. 14, was being operated by
radio remote control at the time of the accident. The remote control unit
was a Matric Model TX-3, S.N. 75205AD013 D, which operated on a carrier
frequency of 458 MHZ. 8.
The remote control unit showed no visible damage. 9.
The light switches were found in the “On” position
with both the area lights and headlights burning. 10.
The following components were removed from the
continuous mining machine involved in the accident for further
testing: ·
Matric Limited Remote Control Demultiplexer, Model:
500-200, P/N 100087264, S/N 90201ADO12B, MSHA IA 457 ·
Matric Limited Permissible Radio Transmitter with
strap, Model TX3 (458 MHz), P/N 100112672,S/N 75205AD013D, MSHA Approval
2G-4096-0 ·
Matric Limited Receiver, Type RX1, P/N 100016248, S/N
83810AC001 D, MSHA IA-18528-0-1br ·
Matric Limited Antenna, P/N 00601843-0251, S/N
5024233-000. ·
Magnetek Firing Package, P/N RP601849-1124, S/N
4040601-001 ·
·
·
Joy tram motor contactor assembly (left), P/N
00601525-0000 ·
Joy tram motor contactor assembly (right), P/N
00601525-0000 ·
Koehler 5000 series cap lamp, with marking “93” 11.
The results of the evaluations and tests that were
performed on the above components are summarized below: A)
The remote control system consisting of the TX3
remote station, victim’s cap lamp and battery, machine-mounted remote
control antenna, remote control receiver, and demultiplexer panel all
functioned properly. The following deficiencies were noted, but were
unlikely to have contributed to the accident: |