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Printer Friendly Version (Contains All Graphics) Jump to Overview DEPARTMENT OF LABOR MINE SAFETY AND HEALTH ADMINISTRATION COAL MINE SAFETY AND HEALTH REPORT OF INVESTIGATION Surface Area of Underground Coal Mine Powered Haulage Accident January 23, 2006 TBK Haulage, Inc. (RCT) Hurley, Virginia at Sassy Coal Co., Inc. No. 4 Biggs, Pike County, Kentucky ID No. 15-17964 Accident Investigator Robert H. Bellamy Mining Engineer Originating Office Mine Safety and Health Administration District 6 100 Fae Ramsey Lane Pikeville, KY 41501 Kenneth A. Murray, District Manager OVERVIEW
Sassy Coal Co., Inc., No. 4, is a one-unit underground coal mine located directly off State Route 1758, one mile north of the intersection of State Route 1758 and State Route 194, at Biggs in Pike County, Kentucky. The principal officer is Charles T. Norman, President. The mine operates one eight-hour shift, five days per week and employs 8 persons. The mine produces approximately 150 tons of coal per day. The coal is transported by truck to the Clintwood Elkhorn Mining Company, Inc, Clintwood Elkhorn #2 preparation plant, located approximately 1.7 miles from the mine. TBK Haulage, Inc. (MSHA Contractor I.D. RCT) is an independent trucking contractor having one coal truck and one employee. The principal officer is Steven Justus, Owner. The last regular safety and health inspection of the mine prior to the accident was completed on December 21, 2005. DESCRIPTION OF ACCIDENT
On Monday, January 23, 2006, at approximately 9:10 p.m., Steven Justus met James Thornsbury at the stockpile area of the Sassy Coal Co., Inc., No. 4 mine in order to assist Thornsbury in adding engine coolant to the Ford LT 9000 coal truck. At that time, Thornsbury was preparing to haul his fourth load of the day to the Clintwood Elkhorn Mining Company, Inc, Clintwood Elkhorn II preparation plant, located approximately 1.7 miles from the mine. Justus returned to the mine office area where he was contacted by phone by John Freeman, mine owner at an adjacent mine, around 10:30 a.m. Freeman informed Justus that he could see the truck on its side near the bottom of the mine haul road with the front end down in the creek. Justus immediately drove down to the accident scene where he found Thornsbury at a location approximately 520 feet from the stockpile loading point. Thornsbury was lying along the edge of the road near the inside edge of the road berm, and approximately 70 feet upgrade of the truck. Justus then returned to the mine office, called 911 for emergency assistance and asked Verlin Taylor, Mine Superintendent, to go to the accident scene and check on Thornsbury. In the mean time, Freeman had contacted Ott Mullins, Manager of Safety and Environmental Affairs for Clintwood Elkhorn Mining Company, Inc, who was also an emergency medical technician (EMT). Upon Mullins' arrival at approximately 10:45 a.m., Justus and Jackie Dotson, a truck driver from the adjacent mine, were also present at the site. Mullins checked Thornsbury for pulse and breathing and observed there were traumatic injuries to Thornsbury's lower torso area indicating he had been run over by the truck. Thornsbury was pronounced dead at 11:51 a.m. by Ernest Casebolt, Pike County Deputy Coroner. INVESTIGATION OF ACCIDENT
Verlin Taylor notified the MSHA Elkhorn City Field Office of the accident at approximately 10:45 a.m. MSHA personnel from the Elkhorn City Field Office and the MSHA District Office in Pikeville, Kentucky, were dispatched to the accident site. A 103(k) Order was issued to secure the accident scene while an investigation was conducted to ensure the safety of any persons at the mine. A mechanical engineer from the MSHA Approval and Certification Center office arrived on January 24, 2006, to conduct a detailed mechanical evaluation of the Ford LT 9000 truck. The investigation was conducted in cooperation with State officials. An interview with the contractor was conducted at the Kentucky Office of Mine Safety and Licensing office in Pikeville, Kentucky on January 26, 2006. DISCUSSION
Haul Road Conditions The mine haul road began at the stockpile area where the truck was loaded by the driver. The mine haul road extended downgrade for a distance of approximately 600 feet where it joined a graveled state road. The overall grade of the mine haul road was 14.1%, according to surveying information provided by Clintwood Elkhorn Mining Company, Inc. The haul road base was well compacted and the surface consisted of graded, limestone gravel. The berm on the outside edge of the road averaged three feet in height. The post-accident visual examination of the haul road revealed no evidence of extreme braking efforts (skid marks) nor evidence that the truck had been in a runaway mode (there was no indication of an attempt to steer the truck into the hillside or the road ditch). Tire tracks that varied from the normal path of travel were visible. The tracks gradually deviated toward the berm on the outside edge of the road starting at a point approximately 75 feet upgrade of the location of the victim. The truck continued traveling in this general direction until it crossed the mine haul road due to encountering a steep curve to the left then went over a gravel berm and into the creek channel. The clearance between the deviating tire tracks and the road berm was 10 feet where the tracks first left the normal route of travel. As the truck continued downgrade, the clearance between the tire tracks and the berm gradually decreased and was measured to be four feet at the location of the victim. Post Accident Position of Truck The post accident position of the truck was nose down in the creek channel and resting on the end of a five-foot steel culvert with the truck rolled over onto its left side. The right rear tandem drive wheels were in the air. Persons interviewed stated that the engine was running and the right drive wheels were turning. Minimal damage occurred to the cab and body of the truck. There was no apparent damage to the interior of the cab. The coal which had been loaded into the truck bed had partially spilled after the truck had turned on its side. No coal spillage was observed except in the immediate area of the truck bed. Mechanical Condition of Truck Relative to Accident The evaluation of the mechanical condition of the truck was conducted by the Approval and Certification Center to determine if any equipment related factors contributed to the accident. The most significant findings relative to whether defects would have caused the truck to enter a runaway mode while traveling down the graded mine haul road are the following:
A functional seat belt was provided in the truck. The seat belt was found to be disengaged and in the stored position. The truck was not equipped with a rollover protection system. Although regulations do not require the use of seat belts in equipment that is not provided with rollover protection, MSHA strongly recommends the use of seat belts in all types of mobile equipment. Mechanical Condition of Driver's Side Cab Door Deficiencies to the window crank handle were identified during the evaluation of the Ford LT 9000 truck. An upward lifting force was required to be applied to the window glass while turning the window crank handle in order to close the window. During the accident investigation, the closing or "rolling up" of the door window was performed while sitting in the driver's seat. The process required reaching across the body with the right hand to grasp the top of the window glass to apply the lifting force, while using the left hand to work the crank handle in a counter-clockwise motion. This action required a shifting of weight and the body to be leaned toward the door. It was noted that the crank handle would intermittently "slip" and in order to achieve meshing with the internal workings of the crank mechanism, it was necessary to back off the crank handle in the clockwise direction and then continue the counter-clockwise cranking motion. The knob was missing from the window crank handle which required the crank to be grasped from the end. The clearance between the end of the window crank handle and the end of the door latch handle was measured to be two inches. The door latch mechanism was operative and properly functioning to hold the door closed. The motion required to release the door latch was an upward lifting motion of the inside latch handle, while the motion to roll up the door window was a counter-clockwise motion. The two motions are converse to one another, but as noted, it was necessary to back off the window crank handle intermittently in a clockwise motion to achieve realignment of the crank mechanism. The effort required to release the door latch was significantly less for the driver's side door than for the passenger side door. The distance from the driver's side door to the outside rear view mirror was 15 inches. Weather It had been raining lightly throughout the morning and at the time of the accident. The temperature was approximately 40 to 45 degrees. Possible Cause of Accident There was no eyewitness to the accident. The following facts and conclusions are presented to develop a basis for the factors contributing to the accident:
After loading the truck in the stockpile area, Thornsbury entered the truck and began driving down the mine haul road. He rolled down the window to clean the rear view mirror mounted to the outside of the door. After cleaning the mirror using folded paper towels, Thornsbury began to roll the window back up. He reached across his body with his right hand to pull up on the window glass while turning the window crank with his left hand. The door latch handle was inadvertently tripped, while his weight was shifted against the door. When the door opened, he fell from the cab of the truck. ROOT CAUSE ANALYSIS
An analysis was conducted to determine the most basic causes of the accident. Listed below are root causes identified during the analysis and their corresponding corrective actions implemented to prevent a recurrence of the accident. Root Cause: The contractor had no policies or procedures to ensure the truck was being maintained in safe condition. A practice of performing routine pre-operational checks had not been established and records of safety examinations or maintenance measures were not maintained. Corrective actions: The contractor has developed an accident prevention policy to require truck drivers to: "do a pre-shift examination of the equipment before moving the equipment on a daily basis. A record of the daily examination is to be kept in the end loader." Root Cause: The contractor had no policy for the use of seat belts. Corrective Actions: The contractor has developed an accident prevention policy which states: "Truck drivers will be required to wear seat belts on mine property when trucks are in motion." CONCLUSION
The accident occurred when the driver fell from the truck while it was in motion. Pre-operational inspections of the truck by a qualified person were not being conducted and defects affecting safety were not recorded and reported to the contractor and corrected before the truck was put in service. The trucking contractor had no policy for the use of seat belts, which were not worn at the time of the accident. ENFORCEMENT ACTIONS
1. A 103(k) Order No. 7424873, was issued on January 23, 2006, to Sassy Coal Co., Inc.
Related Fatal Alert Bulletin: APPENDIX A
Persons Participating in the Investigation Sassy Coal Co., Inc
Verlin Taylor .......... Superintendent
Roger Baker .......... Contract Mechanic
Tracy Stumbo .......... Chief Accident Investigator Ronald Hughes .......... Director of Accident Investigations Mike Elswick .......... District Supervisor
James Salyer .......... Coal Mine Inspector James Hager .......... Supervisory Mine Inspector Robert Hardman .......... Assistant District Manager-Enforcement Timothy Watkins .......... Assistant District Manager-Technical Robert Bellamy .......... Mining Engineer Michael Pruitt .......... Education Field Services |
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