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Jump to Overview DEPARTMENT OF LABOR MINE SAFETY AND HEALTH ADMINISTRATION Metal and Nonmetal Mine Safety and Health REPORT OF INVESTIGATION Underground Mine (Lead and Zinc) Fatal Fall of Ground Accident January 25, 2007 J. S. Redpath Corp.. Contractor I.D. No. R83 at Teck Cominco American Inc Pend Oreille Mine Metaline Falls, Pend Oreille County, Washington Mine I.D. No. 45-00366 Investigators Randy L. Cardwell Supervisory Mine Safety and Health Inspector David J. Small Mine Safety and Health Inspector William J. Gray Mining Engineer Sandin E. Phillipson Geologist Melvin K. Palmer Mine Safety and Health Specialist Originating Office Mine Safety and Health Administration Western District 2060 Peabody Road, Suite 610 Vacaville, California 95687 Arthur L. Ellis, District Manager OVERVIEW
Phillip O. Markhart, underground miner, age 43, was fatally injured on January 25, 2007, while operating a roof bolter. Markhart was installing wire mesh when a large rock fell and struck him. The accident occurred because management failed to design and maintain a ground support system in a manner that would control the ground where the bolter operators were performing their assigned tasks. A bolt sequence to ensure the safe handling and installation of the welded wire ground support panels was not in place at the time of the accident. GENERAL INFORMATION
Pend Oreille Mine, an underground lead and zinc ore operation, owned by Teck Cominco American Inc., was located in Metaline Falls, Pend Oreille County, Washington. The principal operating official was Mark J. Brown, general manager. The mine normally operated two 11-hour shifts per day, five days a week. Total employment was 181 persons. J. S. Redpath Corp.., ( Redpath ) located in Sparks, Washoe County, Nevada, was contracted by the mine operator to develop a portion of the mine's drifts. The principal operating official was Christopher C. Hickey, general manager. A formal agreement specifying the scope of work was finalized in December 2006 and Redpath commenced activities at the Pend Oreille Mine the week of January 8, 2007. Redpath normally worked two 11-hour shifts, five days a week and employed 13 persons at the mine. The rock was drilled, blasted, and moved by front-end loaders and trucks to an underground shaft hoist and then to an underground stockpile area. The material was transported to the surface by conveyor belts where it was processed by a milling operation. The finished products were shipped and sold to commercial industries. The last regular inspection at this operation was completed on December 12, 2006. DESCRIPTION OF ACCIDENT
On January 24, 2007, Phillip O. Markhart, (victim), and Monte Nelson, miner, started to work at 6:30 p.m., in the W83D4J heading (drift). The heading had been loaded and blasted at the end of day shift. After they loaded the shot rock out of the heading with a front-end loader, they brought a roof bolter to the heading to start the bolting cycle. The grade of the heading was too steep for the roof bolter to climb under its own power so a front-end loader was used to push it into position. Nelson and Markhart then began installing wire mesh and rock bolt supports. At approximately 12:30 a.m., on January 25, 2007, Joel Clark, shift boss, entered the heading, talked with the miners, and examined the area. The roof bolter would not climb the heading again but had to be advanced to continue the bolting cycle. Clark operated the front-end loader to push the roof bolter forward so the bolting operation could continue and at approximately 12:45 a.m., he left the work area. Clark had pushed the roof bolter forward to a location that placed a portion of the roof bolter's work platform beyond the last row of bolts previously installed (Appendix D ). The miners then installed one panel of wire mesh on the left rib with two bolts. At approximately 1:00 a.m., as they continued to install wire mesh, a large rock fell from the roof, striking Markhart and pushing Nelson out of the way. Nelson could not remove the rock from the victim so he went into the next drift and got Josh Eoff, driller, to help him. They removed the rock and Nelson called for emergency assistance. Markhart was transported to the surface and then transferred to a local fire station where he was pronounced dead. The cause of death was attributed to blunt force trauma. INVESTIGATION OF THE ACCIDENT
MSHA was notified of the accident at 2:15 a.m., on January 25, 2007, by a telephone call from Brad Davenport, senior safety coordinator, to Steve Cain, supervisory mine safety and health inspector. An investigation was started the same day. An order was issued under the provisions of section 103(k) of the Mine Act to ensure the safety of the miners. MSHA's accident investigation team traveled to the mine, conducted a physical inspection of the accident scene, interviewed employees, and reviewed documents and work procedures relevant to the accident. MSHA conducted the investigation with the assistance of mine management, the contractor, the employees, a miner's representative, the local fire department, and the county sheriff's office. DISCUSSION
Location of the Accident The accident occurred near the face in the Warren zone, the lowest ore body being developed in the mine. The face of W83D4J heading (drift) was approximately 65 feet from the last intersection. The W83D4J heading was being developed by Redpath. They mined this heading beginning approximately 14 feet north of the 3-way intersection defined by the W83D4J and dog-legged W83D5 headings (Appendix B). The original W83D5 heading was narrowed down and split into the W83D5 drift, mined from the mouth to an extent of 65 feet toward the east-northeast and the W83D4J drift, mined approximately 45 feet due North. As measured with the clinometer on a handheld transit, the floor grade along the original, northeast-trending portion of the W83D5 drift was 10-12 degrees (approximately 20 percent grade) into the 3-way intersection. The floor grade increased slightly to 13 degrees from the center of the 3-way intersection to a position approximately 12 feet into the W83D4J drift. This was the approximate position at which Redpath began mining. From this point, the floor grade increased to 18 degrees (33 percent grade) over a distance of approximately 20 feet, before returning to a more moderate grade toward the face. Geological Conditions The geology was characterized by thinly bedded dolomite that strikes northwest and dips 20 degrees toward the southwest, with beds inclined toward the mouth of the W83D4J drift. A prominent, two foot wide, fault zone was exposed in the face, angled from the top, right corner downward to the middle of the face where it intersected the floor. The fault zone strikes approximately N 13 degrees E and dips approximately 67 degrees toward the northwest extending across the back to intersect the left rib about 15 feet from the drift mouth ( Appendix C ). The fault zone was characterized by sheared-out blocks of dolomite, with adjacent bedding planes exhibiting drag motion along the sheared zone. As exposed in the back, the hanging wall block was characterized by a series of closely spaced (2 inches) joints that paralleled the main fault zone. Roof Bolter The roof bolter involved in the accident was manufactured by MacLean Engineering and Marketing Co. of Ontario, Canada. The MacLean model MEM-928 had a rock drill with a scissor lift work platform. The operator's tram compartment was equipped with a Roll-over Protective Structure (ROPS) and a Fall Protective Structure (FOPS) certified canopy. However, the roof bolter's elevated work platform, from where the rock bolts were installed, was not equipped with an operator's canopy or any auxiliary roof support jacks. This work platform was approximately 8-feet wide and 13-feet long featuring both a vertical adjustment of approximately 6 feet via a scissors lift linkage and a front-to-back sump capability of approximately 39 inches. The bolting machine was not equipped with a device to handle the 5 foot by 10 foot wire mesh panels. Loading of the wire mesh onto the top of the drill mast and positioning it prior to bolting, required handling by the miners positioned on the elevated work platform. The bolter had a single, mast-feed style drill boom which inCorp.orated an indexing mechanism with one position for drilling and a second for bolt installation. This design eliminated the need for drill steel handling but still required manual loading of the roof bolt for each installation. Although the roof bolter was a single-boom design and the manufacturer advertised it as a one-man operation, reportedly a two man crew was always used by Redpath. The typical operation involved one operator manning the controls, either at the main valve bank or via a tethered remote unit and the second person acting as a helper handling the bolts and wire mesh panels. MacLean Engineering literature technical specifications listed a maximum grade of 20 percent for the Model 900 series roof bolter. The floor grade where the roof bolter was positioned at the time of the accident exceeded 20 percent. A violation was issued for using the bolter beyond the manufacturer's designed capacity. This violation was not determined to have contributed to the accident. Bolting Cycle The written contract between Teck Cominco American Inc, and Redpath specified that primary ground support would consist of eight-foot Swellex bolts, on a 4 foot by 4 foot pattern with ( 6-gauge, 5-foot-wide by 10- foot-long ) welded wire mesh. Fall of Ground A shallow cavity was exposed in the center of the main fault zone, recognized by freshly exposed joint surfaces that were not coated with dust, and also by poorly developed slickensides. The cavity was approximately 14 feet long, 2 feet wide, and one foot deep. It extended from the right corner of the face and followed the fault zone to the edge of the last panel of unbolted wire mesh. The dimensions of the fall cavity contained an estimated 23 cubic feet of dolomite, weighing approximately 3,800 pounds. The bolter deck was littered with blocky pieces of dolomite ranging in size from 1 inch to 12 inches, in addition to the main piece of intact rock that covered the victim. The largest piece of intact rock on the bolter deck, which had been moved to free the victim, was approximately 5 feet long, 2 feet wide, and 10 inches thick at its maximum, although it tapered slightly to define a wedge-shaped cross section. The intact rock weighed about 1,350 pounds. Drift width varied between 15 to 19 feet, with a height of 18 to 19 feet. The blasting pattern reportedly required the outside blast holes to be drilled at the intended rib line and roof line. Wire mesh bolted to the roof and ribs caught abundant pieces of broken, angular, rough-surfaced rock. Rock fragments ranged in size from 2-24 inches, and were defined by rough fracture surfaces indicative of blasting, rather than by smoother, more regular surfaces that would be indicative of naturally occurring geologic structures. Training and Experience Phillip O. Markhart had seven years of mining experience and one year of experience operating other roof bolters. He began working at this mine on January 24, 2007, and had not received training in accordance with 30 CFR, Part 48. Monte L. Nelson had seven years of mining experience and one year of experience operating a MacLean roof bolter. He began working at this mine on November 29, 2006, and had received training in accordance with 30 CFR, Part 48. ROOT CAUSE ANALYSIS
A root cause analysis was conducted and the following root causes were identified: Root Cause: Management policies and controls were inadequate and did not ensure that newly hired experienced miners were trained before they were assigned to begin work duties. The victim had received site specific training but had not received training on the mine's roof control plan and was unfamiliar with the ground conditions at this mine. Corrective Action: Management should develop and implement plans to train newly hired experienced miners before they are assigned to work. Root Cause: Management policies and controls were inadequate and did not ensure that persons were protected from fall of ground hazards when they were installing wire mesh. The elevated work platform was not equipped with a canopy; the bolting machine was not equipped with a device to handle the wire mesh; roof support jacks were not provided; and a detailed bolt installation sequence was not being utilized to ensure miners were located under supported ground when installing ground support. Corrective Action: Management should establish policies and controls to ensure that persons can safely install ground support. Management should monitor persons conducting the task of installing ground support to ensure that policies and controls are effective in protecting the miners. CONCLUSION
The accident occurred because management failed to design and maintain a ground support system in a manner that would control the ground where the bolter operators were performing their assigned tasks. A bolt sequence to ensure the safe handling and installation of the welded wire ground support panels was not in place at the time of the accident. The failure to train the victim on the mine's roof control plan and to ensure he was familiar with the ground conditions at this mine and understood how to safely install ground support contributed to this accident. ENFORCEMENT ACTION
Teck Cominco American Inc. Order No. 6342331 was issued on January 25, 2007, under the provisions of Section 103 (k) of the Mine Act:
J.S. Redpath Corp. Citation No. 6338476 was issued on March 20, 2007, under the provisions of Section 104(a) of the Mine Act for a violation of 30 CFR 48.6(b):
Citation No. 6338477 was issued on March 20, 2007, under the provisions of Section 104(d) of the Mine Act for a violation of 30 CFR 57.3360:
Related Fatal Alert Bulletin: APPENDIX A
Persons Participating in the Investigation Teck Cominco American Inc
Brad N. Davenport ............... senior safety coordinator Sandy B. McFarlane ............... senior safety coordinator Kevin E. Kinsella ............... environmental health & safety superintendent Mark J. Brown ............... general manager David E. Riggleman ............... mine superintendent Ray W. Bloomer ............... miner's representative Mace G. Thiuierge ............... miner's representative Christine L. Mulligan ............... surveyor
Mark S. Immonen ............... senior manager of operations Fern C. Larosie ............... project superintendent John R. Rhodes ............... mine captain Chris C. Hickey ............... general manager Adele L. Abrams ............... attorney Margaret S. Lopez ............... attorney
David J. Small ............... mine safety and health inspector Ron Eastwood ............... mine safety and health inspector Sandin E Phillipson ............... geologist William J. Gray ............... mining engineer Melvin K. Palmer ............... mine safety and health specialist |
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